Statuts: | Accident investigation report completed and information captured |
Date: | jeudi 6 mai 1971 |
Heure: | 13:15 |
Type/Sous-type: | Carstedt Jet Liner 600A |
Compagnie: | Apache Airlines |
Immatriculation: | N4922V |
Numéro de série: | 04285 |
Année de Fabrication: | |
Moteurs: | 2 Garrett TPE331 |
Equipage: | victimes: 2 / à bord: 2 |
Passagers: | victimes: 10 / à bord: 10 |
Total: | victimes: 12 / à bord: 12 |
Dégats de l'appareil: | Détruit |
Conséquences: | Written off (damaged beyond repair) |
Lieu de l'accident: | 8 km (5 milles) SW of Coolidge, AZ ( Etats-Unis d'Amérique)
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Phase de vol: | En vol (ENR) |
Nature: | Transport de Passagers Nat. |
Aéroport de départ: | Tucson International Airport, AZ (TUS/KTUS), Etats-Unis d'Amérique |
Aéroport de destination: | Phoenix-Sky Harbor International Airport, AZ (PHX/KPHX), Etats-Unis d'Amérique |
Numéro de vol: | 33 |
Détails:The purpose of the accident flight was as a normally scheduled air taxi flight between Tucson (KTUS) and Phoenix (KPHX), USA. The flight was operated by Apache Airlines, Inc. The aircraft crashed about 5 miles southwest of Coolidge. The accident aircraft, a De Havilland Dove, was originally produced with two reciprocating engines and seating for ten passengers and two pilots. The accident aircraft had been altered under a Supplemental Type Certificate (STC) that replaced the engines with Garret TPE-331 turboprop engines and lengthened the fuselage, allowing seating for 18 passengers. As part of this STC conversion, the wing lower main root joint fittings, which was done to accommodate the new engines as well as changes to the fuel system; the fittings were included with the alteration, and were made of heat treated alloy steel. This STC was developed by the Von Carstedt Corporation of Long Beach, California.
Witnesses to the accident reported initially seeing the aircraft flying on a northwesterly heading. Engine noises were heard to suddenly cease, and the aircraft began a shallow descent. The descent steepened into a 40-50 degree dive. The aircraft soon struck a freshly plowed agricultural field. The main wreckage and right wing came to rest 35 feet apart. A wing root fairing was located 1,160 feet downwind of the main wreckage. Investigation revealed the right wing lower main root joint fitting had failed in fatigue, causing the wing to begin to separate in flight, eventually departing the aircraft completely after the aircraft had entered an emergency descent. The fatigue failure of the fitting occurred because the size and geometry of the fitting did not allow the complete and consistent hardening of the material throughout its thickness, causing soft areas within the part. Corrosion and fretting damage was also noted on the fitting.
Probable Cause:
Probable Cause: "The inflight failure and subsequent separation of the right wing. This failure was the result of a fatigue fracture in the lower main root joint fitting which propagated from an area of corrosion and fretting damage which, in turn, was caused by design deficiencies. These deficiencies remained undetected because surveillance of the supplemental type certification process and the modification programs was not adequate to assure compliance with design and inspection requirements."
Accident investigation:
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Investigating agency: | NTSB  |
Status: | Investigation completed |
Duration: | 1 year | Accident number: | NTSB-AAR-72-19 | Download report: | Final report
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Opérations de secours
NTSB issued 3 Safety Recommendations
Issued: 12-MAY-1971 | To: | A-71-31 |
CONDUCT A ONE-TIME METALLURGICAL INSPECTION ON AN EXPEDITED BASIS BY APPROVED METHODS OF ALL LOWER MAIN WING SPAR ROOT FITTINGS P/N CPD2004 ON ALL DE HAVILLAND MODEL DH.104 "DOVE" AIRPLANES THAT HAVE BEEN MODIFIED UNDER STC NO. SA1747WE. (Closed - Acceptable Action) |
Issued: 12-MAY-1971 | To: | A-71-32 |
REVIEW THE ADEQUACY OF AIRWORTHINESS DIRECTIVE 70-15-6 AND REVISE AS NECESSARY TO ASSURE ADEQUATE SERVICE LIMITS ON THIS FITTING. (Closed - Acceptable Action) |
Issued: 23-JUN-1971 | To: | A-72-115 |
(A)CONDUCT A ONE-TIME METALLURGICAL INSPECTION ON AN EXPEDITED BASIS BY APPROVED METHODS OF ALL LOWER MAIN WING SPAR ROOT FITTINGS P/N CPD-2004 ON ALL DEHAVILLAND MODEL DH-104 "DOVE" AIRPLANES THAT HAVE BEEN MODIFIED UNDER STC NO. SA1747WE. (B) REVIEW THE ADEQUACY OF AIRWORTHINESS DIRECTIVE 70-15-6 AND REVISE AS NECESSARY TO ASSURE ADEQUATE SERVICE LIMITS ON THIS FITTING. (Closed - Unacceptable Action) |
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Photos

accident date:
06-05-1971type: Carstedt Jet Liner 600A
registration: N4922V
Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Tucson International Airport, AZ et Phoenix-Sky Harbor International Airport, AZ est de 176 km (110 miles).
Accident location: Approximate; accuracy within a few kilometers.
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.