Narrative:TWA Flight 841 entered an uncontrolled maneuver at FL390. The aircraft descended to about 5,000 feet in about 63 seconds before the flightcrew regained control. About 22:31, the flightcrew made an emergency landing at Detroit.
The flight was cruising in visual flight conditions at night at FL390 when the uncontrolled maneuver began; there was no turbulence. There was a cloud layer near FL200 and, at 21:55, the reported weather at Saginaw was 500-foot overcast with 3 miles visibility in light snow; small breaks were reported in the overcast. Analysis of the evidence indicated that the uncontrolled maneuver began about 2147:47 with isolation of the aircraft's No. 7 leading edge slat (on its right wing) in the extended or partially extended position. During the preceding 14 seconds, the aircraft had rolled slowly to the right to about 35° of right bank and was returned to near wings level flight. Thereafter, the aircraft rolled again to about 35° of right bank in about 4 seconds. About 2147:51, the right roll was stopped near 35° of bank for a few seconds. At that time, the aircraft reached a condition wherein Mach number, angle of attack, and sideslip combined to reduce the aircraft's lateral control margin to zero or less, and the aircraft continued to roll to the right in a descending spiral. During the following 33 seconds, the aircraft completed 360° of roll while descending to about 21,000 feet. The aircraft entered a second roll to the right during which the No. 7 slat was torn from the aircraft. Control of the aircraft was regained about 21:48:58 at an altitude of about 8,000 feet.
Probable Cause:
PROBABLE CAUSE: "The isolation of the No. 7 leading edge slat in the fully or partially extended position after an extension of the Nos. 2, 3, 6, and 7 leading edge slats and the subsequent retraction of the Nos. 2, 3, and 6 slats, and the captain's untimely flight control inputs, to counter the roll resulting from the slat asymmetry. Contributing to the cause was a pre-existing misalignment of the No. 7 slat which, when combined with the cruise condition airloads, precluded retraction of that slat. After eliminating all probable individual or combined mechanical failures or malfunctions which could lead to slat extension, the Safety Board determined that the extension of the slats was the result of the flightcrew's manipulation of the flap/slat controls. Contributing to the captain's untimely use of the flight controls was distraction due probably to his efforts to rectify the source of the control problem."
A.o. the ALPA did not agree with the NTSB findings. A complex interaction that involved the tightly coupled response of lateral and directional flight controls on the B727-100 aircraft was claimed to have caused the accident.
Accident investigation:
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Investigating agency: | NTSB |
Status: | Investigation completed |
Duration: | 2 years and 2 months | Accident number: | NTSB/AAR-81-8 | Download report: | Final report
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Classification:
Loss of control
Sources:
» Flight International 1-7 February 1995(25)
Follow-up / safety actions
NTSB issued 1 Safety Recommendation
Issued: 17-JAN-1980 | To: FAA | A-80-8 |
DISSEMINATE TO ALL BOEING 727 OPERATORS AND FLIGHTCREWS INFORMATION OF THE TYPE INCLUDED IN BOEING OPERATIONS MANUAL BULLETIN 75-7 AND TWA FLIGHT OPERATIONS SAFETY BULLETIN 79-3 WHICH ADDRESS CONTROL PROBLEMS ASSOCIATED WITH HIGH-SPEED ASYMMETRICAL LEADING EDGE SLAT CONFIGURATION ON B-727 AIRCRAFT. (Closed - Reconsidered) |
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Map
This map shows the airport of departure and the intended destination of the flight. The line between the airports does
not display the exact flight path.
Distance from New York-John F. Kennedy International Airport, NY to Minneapolis-St. Paul International Airport, MN as the crow flies is 1640 km (1025 miles).
This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.