Statuts: | Accident investigation report completed and information captured |
Date: | mercredi 13 juin 1984 |
Heure: | 16:56 |
Type/Sous-type: |  McDonnell Douglas DC-9-31 |
Compagnie: | USAir |
Immatriculation: | N964VJ |
Numéro de série: | 47373/522 |
Année de Fabrication: | 1969 |
Moteurs: | 2 Pratt & Whitney JT8D-7B |
Equipage: | victimes: 0 / à bord: 5 |
Passagers: | victimes: 0 / à bord: 51 |
Total: | victimes: 0 / à bord: 56 |
Dégats de l'appareil: | Substantiels |
Conséquences: | Repaired |
Lieu de l'accident: | Detroit-Metropolitan Wayne County Airport, MI (DTW) ( Etats-Unis d'Amérique)
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Phase de vol: | A l'atterrissage (LDG) |
Nature: | Transport de Passagers Nat. |
Aéroport de départ: | Hartford-Brainard Airport, CT (HFD/KHFD), Etats-Unis d'Amérique |
Aéroport de destination: | Detroit-Metropolitan Wayne County Airport, MI (DTW/KDTW), Etats-Unis d'Amérique |
Détails:A McDonnell Douglas DC-9-31 operated by USAir, suffered a landing accident at Detroit-Metropolitan Airport, MI.
During arrival, the aircrew noted thunderstorms west & southwest of the airport. The crew elected to continue and make an ILS approach. At 16:36, a special weather observation had thunderstorm info, but was not noted. At 16:50, the visibility dropped to 1/4 mi with heavy rain and hail. As the aircraft approached runway 21R, a VIP Level 4 thunderstorm moved from west to east over the northern part of the airport. The controller provided wind info from the low level wind shear alert system (LLWAS), but used improper phraseology and failed to provide RVR information when the visibility went below 1 mile. The crew had difficulty in understanding the LLWAS info due to the amount and rapidity that it was provided. At approx 350 feet agl, the aircraft encountered low clouds, heavy rain, hail and turbulence. The aircrew initiated a missed approach. The speed increased to 143 kts, then decreased to approx 119 kts. The captain believed the aircraft would not climb and elected to land. The aircraft touched down about 2500 feet down the runway with the gear partially extended, then slid 3800 feet and went off the runway. The wind was gusting to 32 kts.
Probable Cause:
Probable Cause: "Inadequate cockpit coordination and management which resulted in the captain's inappropriate decision to continue the instrument approach into known thunderstorm activity where the airplane encountered severe wind shear. The failure of air traffic control personnel at the airport to provide additional available weather information deprived the flightcrew of information which may have enhanced their decisionmaking process."
Accident investigation:
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Investigating agency: | NTSB  |
Status: | Investigation completed |
Duration: | 265 days (9 months) | Accident number: | NTSB/AAR-85/01 | Download report: | Final report
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Sources:
» NTSB
Opérations de secours
NTSB issued 2 Safety Recommendations
Issued: 15-APR-1985 | To: FAA | A-85-26 |
IN COOPERATION WITH AIR CARRIERS AND MANUFACTUERS DEVELOP A COMMON WIND SHEAR TRAINING PROGRAM, AND REQUIRE AIR CARRIERS TO MODIFY AIRLINE TRAINING SYLLABI TO EFFECT SUCH TRAINING. (Closed - Acceptable Action) |
Issued: 15-APR-1985 | To: FAA | A-85-27 |
CONDUCT RESEARCH TO DETERMINE THE MOST EFFECTIVE MEANS TO TRAIN ALL FLIGHTCREW MEMBERS IN COCKPIT RESOURCE MANAGEMENT, AND REQUIRE AIR CARRIERS TO APPLY THE FINDINGS OF THE RESEARCH TO PILOT TRAINING PROGRAMS. (Closed - Acceptable Action) |
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Photos
Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Hartford-Brainard Airport, CT et Detroit-Metropolitan Wayne County Airport, MI est de 880 km (550 miles).
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.