Accident Lockheed PV-1 Ventura VH-SFF,
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ASN Wikibase Occurrence # 324334
 
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Date:Monday 18 November 1996
Time:13:35
Type:Silhouette image of generic L37 model; specific model in this crash may look slightly different    
Lockheed PV-1 Ventura
Owner/operator:RAAF Museum
Registration: VH-SFF
MSN: 5378
Year of manufacture:1943
Fatalities:Fatalities: 0 / Occupants:
Aircraft damage: Substantial, written off
Category:Accident
Location:3 km SE of Richmond RAAF Base, NSW -   Australia
Phase: Approach
Nature:Demo/Airshow/Display
Departure airport:Richmond RAAF Base, NSW (XRH/YSRI)
Destination airport:Richmond RAAF Base, NSW (XRH/YSRI)
Investigating agency: BASI
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The aircraft was approaching to land after completing a handling display during an Open Day at RAAF Richmond. At an altitude of about 800ft, on the base leg for runway 28, both engines stopped simultaneously and without warning. As there was insufficient altitude to reach the field for a power off landing, the flaps and landing gear were retracted and a successful forced landing carried out into a cleared field short of the airfield. The crew evacuated the aircraft without injury.
A subsequent investigation failed to positively determine the cause of the simultaneous stoppage of both engines. A large quantity of fuel remained in the tanks and no defects were found with either of the engine fuel systems. The engine ignition systems were tested and functioned normally after the accident.
The design of this aircraft, as with other ex-military multi-reciprocating engine types, includes a master ignition switch. The switch is guarded, and when turned off results in the termination of ignition to all engines simultaneously. The switch was removed from the aircraft after the accident and subjected to extensive testing, including vibration tests, but could not be faulted. It was noted however that ignition isolation resulted with only a small movement of the switch from the ON position.
The most likely reason for the sudden stoppage of both engines was movement of the master ignition switch from the ON position, possibly as the result of vibration or by a crew member inadvertently bumping the switch prior to landing.

Accident investigation:
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Investigating agency: BASI
Report number: 199603738
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:


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