Statuts: | |
Date: | vendredi 22 novembre 1996 |
Heure: | ca 19:30 |
Type/Sous-type: |  Lockheed HC-130P Combat King |
Compagnie: | United States Air Force - USAF |
Immatriculation: | 64-14856 |
Numéro de série: | 4072 |
Année de Fabrication: | 1965 |
Equipage: | victimes: 10 / à bord: 11 |
Passagers: | victimes: 0 / à bord: 0 |
Total: | victimes: 10 / à bord: 11 |
Dégats de l'appareil: | Perte Totale |
Conséquences: | Written off (damaged beyond repair) |
Lieu de l'accident: | 64 km (40 milles) W de Cape Mendocino, CA, USA ( Océan Pacifique)
|
Phase de vol: | En vol (ENR) |
Nature: | Militaire |
Aéroport de départ: | Portland International Airport, OR (PDX/KPDX), Etats-Unis d'Amérique |
Aéroport de destination: | San Diego-North Island NAS, CA (NZY/KNZY), Etats-Unis d'Amérique |
Détails:The Lockheed HC-130P Combat King aircraft departed Portland International Airport, Oregon, USA at 17:20 PST on an instrument flight rules (IFR) flight en route to North Island Naval Air Station at San Diego, California. The purpose of the sortie was to conduct an overwater navigation evaluation. The aircraft, with callsign 'King 56', began the sortie with a normal takeoff, departure and climbout. One hour and 24 minutes after takeoff in level flight at FL 220 the mishap sequence began with the engineer commenting on a torque flux on the number 1 engine. Over the next three minutes, the operations of all four engines became unstable and eventually failed.
The engineer called for number 1 propeller to be placed in mechanical governing. This would normally remove electrical inputs to the propeller through the synchrophaser. The pilot then called for all four propellers to be placed in mechanical governing. This action was consistent with treating this emergency as a four-engine rollback. There is no indication on the DFDR or the CVR as to whether or not the crew selected mechanical governing on any of the remaining three propellers. At the same time the crew was analyzing the emergency, they also declared an in-flight emergency with Oakland ARTCC and turned the mission aircraft east to proceed toward Kingsley Field, Klamath Falls, Oregon, approximately 230 miles away and approximately 80 miles from the coast. The Radio Operator radioed the USCG Humboldt Bay Station and notified them of the in-flight emergency. During the turn toward the shore the number 3 and number 4 engines once briefly recovered most of their torque. These increases are recorded by the flight data recorder. When the RPM on number 3 (the aircraft’s last functioning engine) finally decreased below 94% RPM the last generator producing electrical power dropped off line due to low frequencies. As a result, at 18:46 Pacific Standard Time all electrical power was lost. After a brief period, power was restored to the equipment powered by the battery bus. From this point on, the aircraft glided to the attempted ditching.
Probable Cause:
Cause: Fuel starvation.
Sources:
»
C-130 Broad Area Review (January 1998)
Photos
Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Portland International Airport, OR et San Diego-North Island NAS, CA est de 1495 km (934 miles).
Accident location: Global; accuracy within tens or hundreds of kilometers.
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.