ASN Wikibase Occurrence # 323406
Date: | Thursday 19 October 2000 |
Time: | 15:38 |
Type: | Beechcraft 300 Super King Air |
Owner/operator: | AeroSmith Aviation |
Registration: | N398DE |
MSN: | FA-109 |
Year of manufacture: | 1986 |
Total airframe hrs: | 3801 hours |
Engine model: | Pratt & Whitney Canada PT6A-60A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed, written off |
Category: | Accident |
Location: | Concord-Buchanan Field, CA (CCR) -
United States of America
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Phase: | Take off |
Nature: | Ferry/positioning |
Departure airport: | Concord-Buchanan Field, CA (CCR/KCCR) |
Destination airport: | San Jose Municipal Airport, CA (SJC/KSJC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Beechcraft 300 Super King Air twin-engine airplane, N398DE, overran the runway and struck an automobile during an aborted takeoff at the Concord-Buchanan Field, CA (CCR). The airplane sustained substantial damage; however, the airline transport pilot sustained minor injuries. The driver, who was the sole occupant of the automobile, received serious injuries. The airplane was registered to King Air Charter was operated by AeroSmith Aviation as a positioning flight when the accident occurred. The flight was originating at the time of the accident and was destined for San Jose Municipal Airport, CA (SJC). Visual meteorological conditions prevailed, and a flight plan was not filed.
According to the pilot's written statement, he performed a rolling takeoff on runway 32R and was paying close attention to balancing the engine power and keeping runway centerline alignment. As the airplane accelerated, the pilot set the engine power above 80 percent and began an instrument scan. He then noted the airspeed indicator was reading zero with the needle resting on the peg. The pilot looked back at the power (torque) gauges, and then back to the airspeed indicator. He then attempted to abort the takeoff by reducing the power levers to idle, then to reverse, and by applying the brakes.
The airplane skidded off the end of the runway, through a chain link perimeter fence, and struck an automobile that was traveling on the perimeter road. The airplane continued across the road, coming to rest on second chain link fence that bordered California State Highway 4.
After coming to a stop, the pilot moved the fuel control levers to fuel cutoff, closed the engine firewall fuel shutoff valves, and moved the gang bar down to shutoff all electrical power. He then deplaned through the aft main cabin door.
PROBABLE CAUSE: "The pilot's delayed decision to abort the takeoff and his failure to utilize the propeller's reverse pitch function."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | LAX01LA019 |
Status: | Investigation completed |
Duration: | 3 years 1 month |
Download report: | Final report |
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Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
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