Runway excursion Accident Dassault Falcon 20C N165TW,
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Date:Sunday 21 December 2008
Time:01:00
Type:Silhouette image of generic FA20 model; specific model in this crash may look slightly different    
Dassault Falcon 20C
Owner/operator:Ameristar Jet Charter
Registration: N165TW
MSN: 65
Year of manufacture:1966
Total airframe hrs:16360 hours
Engine model:General Electric CF700-2D2
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed, written off
Category:Accident
Location:Chautauqua County-Jamestown Airport, NY (JHW) -   United States of America
Phase: Landing
Nature:Cargo
Departure airport:Tulsa International Airport, OK (TUL/KTUL)
Destination airport:Chautauqua County-Jamestown Airport, NY (JHW/KJHW)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The Dassault Falcon 20C, N165TW, was substantially damaged following a runway excursion after landing on runway 25 at the Chautauqua County-Jamestown Airport (JHW), New York. Instrument meteorological conditions prevailed at the time, and an instrument flight rules flight plan was filed for a cargo flight from Tulsa International Airport (TUL), Oklahoma.
The co-pilot was performing a nighttime approach and landing to runway 25. No runway condition reports were received by the flight crew while airborne, and a NOTAM was in effect, stating, "thin loose snow over patchy thin ice." After landing, the co-pilot called out that the airplane was sliding and the wheel brakes were ineffective. The captain took the controls, activated the air brakes, and instructed the co-pilot to deploy the drag chute. The crew could not stop the airplane in the remaining runway distance and the airplane overran the runway by approximately 100 feet. After departing the runway end, the landing gear contacted a snow berm that was the result of earlier plowing. The captain turned the airplane around and taxied to the ramp. Subsequent inspection of the airplane revealed a fractured nose gear strut and buckling of the fuselage. The spring-loaded drag chute extractor cap activated, but the parachute remained in its tail cone container. Both flight crewmembers reported that the runway was icy at the time of the accident and braking action was "nil."
The airport manager reported that when the airplane landed, no airport staff were on duty and had not been for several hours. He also reported that when the airport staff left for the evening, the runway conditions were adequate. The runway had been plowed and sanded approximately 20 hours prior to the accident, sanded two more times during the day, and no measurable precipitation was recorded within that time frame. The reason that the drag chute failed to deploy was not determined.

PROBABLE CAUSE: "The inability to stop the airplane on the remaining runway because of icy runway conditions. A factor was the failure of the drag chute to properly deploy."

Accident investigation:
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Investigating agency: NTSB
Report number: ERA09LA282
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB

Location

Revision history:

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