ASN Wikibase Occurrence # 320078
Date: | Thursday 12 May 2016 |
Time: | 14:13 |
Type: | Cessna 208B Grand Caravan |
Owner/operator: | Parachute Center |
Registration: | N1114A |
MSN: | 208B0309 |
Year of manufacture: | 1992 |
Total airframe hrs: | 12848 hours |
Engine model: | Pratt & Whitney Canada PT6A-42A |
Fatalities: | Fatalities: 0 / Occupants: 18 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | ca 0,6 km E of Lodi Airport, CA -
United States of America
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Phase: | Initial climb |
Nature: | Parachuting |
Departure airport: | Lodi Airport, CA |
Destination airport: | Lodi Airport, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Cessna 208B Grand Caravan (Blackhawk VY conversion) sustained substantial damage in a forced landing in a vineyard, shortly after takeoff from Lodi Airport, California. The pilot suffered a minor injury, but none of the 17 skydivers on board were injured.
The pilot reported that following takeoff from runway 26, he made a right turn and continued his climb for the skydive drop, however, while passing through 1,000 feet above ground level, the engine lost power. The pilot initiated a turn toward the airport, however, realized he was unable to make it, and landed in an open field. During the landing roll, the airplane exited the field, crossed E Jahant Road, impacted a truck, continued into a vineyard, and nosed over.
Postaccident examination of the engine revealed that the fuel pressure line that connects the fuel control unit to the airframe fuel pressure transducer was fractured below the fuel control unit fitting's swaged seat. In addition, a supporting clamp for the fuel pressure fuel line was fractured and separated. The operator reported that the fractured fuel line had been replaced the night before the accident and had accumulated about 4 hours of operational time. The previously-installed line had also fractured.
Probable Cause and Findings: "A total loss of engine power due to a fatigue fracture of the fuel pressure line that connected the
fuel control unit and the fuel flow transducer due to vibration as the result of a fatigue fracture of an associated support clamp. Contributing to the accident was the mechanic's inadequate inspection of the fuel line support clamp during the previous replacement of the fuel line."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | WPR16LA107 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
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Sources:
ABC LA Times NTSB
Location
Revision history:
Date/time | Contributor | Updates |
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