Loss of control Accident Cessna 310R N310JR,
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ASN Wikibase Occurrence # 121065
 
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Date:Friday 11 March 2011
Time:13:43
Type:Silhouette image of generic C310 model; specific model in this crash may look slightly different    
Cessna 310R
Owner/operator:Hudson Management Corporation
Registration: N310JR
MSN: 310R1253
Year of manufacture:1977
Total airframe hrs:5516 hours
Engine model:Continental IO 520 SERIES
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Smyrna, Tennesse -   United States of America
Phase: En route
Nature:Ferry/positioning
Departure airport:Smyrna Airport, TN (MQY/KMQY)
Destination airport:Smyrna Airport, TN (MQY/KMQY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Shortly after departure, the airplane entered a rapid, full-power, near-vertical descent from about 2,700 feet above ground level to ground impact. The elevator trim actuator was found in the full tab-up or airplane nose-down position after the accident. The flight was the second flight of the day and was the fourth in a series of maintenance acceptance flights after the installation of a new avionics suite and a new autopilot system. Before the accident flight, all of the features of the autopilot system tested satisfactorily on the ground but did not yet function as designed in flight, as the airplane demonstrated a pitch-porpoise tendency when the altitude hold feature was engaged.

According to the technician who performed the installation and troubleshooting work on the airplane, he had accompanied the pilot on the first flight that day and had spoken to an autopilot manufacturing representative upon their return. Another troubleshooting procedure was performed, the technician left for lunch, and the pilot departed alone on the accident flight. When describing a previous test flight, the technician stated that the pilot worked the yoke against the autopilot, and, in response, the autopilot ran the elevator trim to the full nose-down position. The pilot responded by swiping both panel-mounted master switches to the off position (autopilot on/off switch and the trim on/off switch) then attempting to trim the airplane with the electric trim that he had just disabled. According to the technician, the pilot yelled at him to turn the system off, and the technician responded that it was off. He said that the pilot’s actions scared him and demonstrated to him that the pilot really didn't have control of the airplane. He noted that, "After the flight, I told [the pilot] he needed to go back and get in the books and learn to operate the system. He seemed very disoriented with the new technology on this flight and previous flights."

Based on the available evidence, it is likely that, after autopilot engagement, the airplane pitched down as a first action of the pitch porpoise, which may have still existed as a discrepancy in the autopilot operation. In response to the downward movement of the airplane, the pilot likely pulled back on the yoke in an effort to arrest the airplane's descent. As a result, the autopilot would have commanded the trim further toward the nose-down position. Such a scenario would require a greater and ever-increasing physical effort by the pilot to overcome the growing aerodynamic force that would result from the nose-down pitch and increasing speed of the airplane. The pilot may have removed one hand from the yoke to again reach for the panel-mounted trim and/or autopilot master switches. With that action, discounting any physical problem, he may have lost his single-handed grip on the control yoke, and the airplane descended in an unrecoverable nose-down attitude.
Probable Cause: The pilot's improper response to a known autopilot pitch divergence anomaly. Contributing to the accident was the pilot's decision to perform a test flight on a system for which he lacked a complete working knowledge.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11FA185
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
11-Mar-2011 17:58 bizjets101 Added
12-Mar-2011 08:17 bizjets101 Updated [Total fatalities, Total occupants, Source]
17-Mar-2011 14:58 harro Updated [Embed code]
09-Feb-2012 01:01 Anon. Updated [Total fatalities, Total occupants, Source, Embed code]
09-Feb-2012 01:02 harro Updated [Time, Nature, Departure airport, Destination airport, Source, Embed code, Narrative]
09-Feb-2012 01:02 harro Updated [Phase, Embed code]
11-Mar-2012 16:02 Geno Updated [Time, Source, Narrative]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 16:45 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]
12-Mar-2024 18:33 Anon. Updated [Nature, Departure airport, Destination airport]

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