ASN Wikibase Occurrence # 133566
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Date: | Friday 22 August 1997 |
Time: | 14:30 LT |
Type: | Cessna 210E |
Owner/operator: | Henry Gantner |
Registration: | N1808F |
MSN: | 210-58708 |
Year of manufacture: | 1965 |
Total airframe hrs: | 2376 hours |
Engine model: | Continental IO-520-A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Oxnard, CA -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Camarillo, CA (KCMA) |
Destination airport: | Burbank, CA (KBUR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During departure climbout, after reaching 1,500 to 2,000 feet agl, the pilot/flight instructor noted that the student pilot had not properly set the throttle friction lock and the throttle had retarded to about 15 inches of manifold pressure. The pilot instructed his student to advance the throttle, however, when the student did so the manifold pressure rose momentarily and then the engine abruptly stopped delivering power. The pilot took control of the aircraft from his student, performed the engine failure checklist, declared an emergency, and established a glide toward a nearby airport. When it became apparent that the aircraft could not glide to the airport, he turned toward an open agricultural field. The aircraft impacted the roof of a house and a light pole across the street from the field boundary and came to rest at the edge of the field. Postaccident examination revealed that a fuel supply hose had come unscrewed off the inlet nipple of the fuel control unit. An 100-hour inspection was completed the prior day and this was the first flight following the inspection.
Probable Cause: The failure of maintenance personnel to properly secure a fuel supply line during a 100-hour inspection and the failure of inspection personnel to detect the loose fitting.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX97LA299 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX97LA299
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 13:20 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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