ASN Wikibase Occurrence # 133622
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 10 May 1997 |
Time: | 13:03 LT |
Type: | American Aviation AA-1 Yankee |
Owner/operator: | Frank G. Fortmann |
Registration: | N5734L |
MSN: | 0134 |
Year of manufacture: | 1969 |
Total airframe hrs: | 1571 hours |
Engine model: | Lycoming O-235-2C2 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Lewisburg, WV -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Middletown, NJ (N92 |
Destination airport: | Beckly, WV (KBKW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was en route to his destination with a planned stopover airport. Due to weather, the pilot switched his stopover airport and obtained the local weather. At that time, the pilot checked the right fuel tank and found it half full. Minutes later, the right fuel tank sight gauge indicated empty. Not sure how much fuel was onboard, the pilot radioed Air Traffic Control and stated that he was fuel critical. Shortly afterwards, the engine lost power and the pilot switched to the left tank. After a brief period, the engine lost power once again, and the pilot switched back to the right fuel tank. The engine produced power for a short period, and then lost power once more. Unable to restart the engine, the pilot executed a forced landing to a small pasture. The left main and nose gears collapsed on impact and the airplane slid through a wooden post supporting a metal wire fence coming to rest upright, on the reciprocal heading. Inspection of the engine found no anomalies. No useable fuel was found onboard. The right fuel tank cap was missing and was not found in the impact area.
Probable Cause: The pilot's inadequate preflight, which led to the loss of a fuel cap and subsequent fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD97LA074 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB IAD97LA074
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 15:32 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation