ASN Wikibase Occurrence # 133780
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 25 March 1998 |
Time: | 23:00 LT |
Type: | Rans S-14 Airaile |
Owner/operator: | Louis Ridge Duskin |
Registration: | N22LD |
MSN: | 1296094 |
Engine model: | Rotax 582 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Hemet, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (KHMT) |
Destination airport: | (KHMT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot lost control of his aircraft during landing and crashed into a mud bog. A sheriff's deputy heard the engine stop and drove to the crash site. He asked the pilot, the only person at the aircraft, if he was hurt. The pilot replied that he wasn't hurt in the landing and that he'd recover his aircraft in the morning. A few minutes later the deputy was contacted by a police officer that had arrested a man for driving while under the influence (DUI). The man had said that his aircraft had been stolen and then had crashed at the airport. The officer brought the man to the hangar and the deputy identified him as the man he had spoken with earlier. The man, now identified by name, also acknowledged that he was the same person the deputy had spoken with at the crash site. He later reported to the FAA that he had gone to eat and had left his hangar open and when he returned, he found his aircraft missing. He ran around the airport looking for it until he saw the aircraft's tail sticking out of a bog. He ran toward it but tripped and fell several times. He decided to tow it to his hangar that night so he drove into town to buy a rope. While en route, he was arrested for DUI. He was held for several hours, then taken to the hospital for a blood test and treatment of his injuries. His blood alcohol was found to be .07% (W/V).
Probable Cause: the pilot's loss of aircraft control during landing, and his physical impairment from a blood alcohol level of 0.07 percent 2 hours following the accident.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX98LA145 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB LAX98LA145
Location
Revision history:
Date/time | Contributor | Updates |
11-Nov-2012 05:30 |
harro |
Updated [Aircraft type, Narrative] |
11-Nov-2012 05:32 |
harro |
Updated [Aircraft type] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Apr-2024 14:16 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation