ASN Wikibase Occurrence # 133788
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Date: | Monday 1 June 1998 |
Time: | 16:32 LT |
Type: | Piper PA-30-320 Twin Comanche C |
Owner/operator: | Leonard M. Lancaster |
Registration: | N7794Y |
MSN: | 30-877 |
Year of manufacture: | 1965 |
Total airframe hrs: | 4197 hours |
Engine model: | Lycoming IO-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | 30 miles SW of Roanoke Airport, near Floyd, Virginia -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Concorde, NC (3N8) |
Destination airport: | Lewisburg, WV (KLWB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:In cruise flight at 10,500 feet, the pilot reported a loss of engine power on one engine and requested vectors to an airport approximately 40 miles away. The controller offered vectors to any of three airports closer to the airplane's position. The pilot declined the offer and repeated his initial request. The airplane subsequently lost power in both engines and crashed approximately 30 miles prior to the requested airport. Examination revealed an undetermined amount of fuel in both outboard auxiliary fuel tanks. Both inboard main fuel tanks contained no evidence of fuel. The cockpit area revealed each fuel selector was in the 'Main' position. The two main tanks held a total of 60 gallons, of which 6 gallons were unusable. Performance charts for the airplane revealed that in cruise flight at 10,500 feet, the airplane consumed approximately 15 gallons of fuel per hour. Examination of the airplane's rental and fueling records revealed the it had flown approximately 4 hours since the last fuel service and had completed at least 5 takeoffs and landings. Examination of the fuel system revealed no defects and both engines ran to rated power in a test cell.
Probable Cause: The pilot's improper selection of fuel tank position resulting in fuel starvation of both engines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD98LA065 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB IAD98LA065
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7794Y 3.
https://flightaware.com/resources/registration/N7794Y Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Apr-2017 22:45 |
Dr.John Smith |
Updated [Time, Aircraft type, Location, Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 11:18 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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