ASN Wikibase Occurrence # 133912
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Date: | Friday 24 November 1995 |
Time: | 15:15 LT |
Type: | Mcclung SEA HAWK |
Owner/operator: | Richard Mcclung |
Registration: | N391SP |
MSN: | 36 |
Total airframe hrs: | 178 hours |
Engine model: | Lycoming O-320-A3B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Marengo, IL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Belvidere, IL (C77) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that approximately 10 minutes into the flight a 'thump' was heard from the right rear of the airplane. He stated that besides a slight list to the right, he did not notice anything unusual with the airplane's flying characteristics. He decided to make a precautionary landing after noticing a rapid depletion of indicated fuel quantity on the upper wing tank gauge. After landing, the pilot and passenger exited the airplane and realized the airplane's upper right wing had departed the airplane. A fire started and consumed the entire airplane. The wing was found 7/8 mile from the resting point of the airplane. Examination of the failed upper right wing, revealed the wing had failed due to compression failure. The investigation also revealed that the failure was due to the presence of unbonded areas between the spar cap and the bidirectional fiberglass that secures the web to the cap. It is not possible to inspect these areas because they are not accessible after construction.
Probable Cause: the failure of the upper right wing due to the presence of unbonded areas between the spar cap and the bidirectional fiberglass. The unbonded areas were due to the inadequate manufacturing of the airplane by the owner/builder. A factor in the accident was the inadequate design by the kit manufacturer.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI96LA041 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB CHI96LA041
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 10:52 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Source, Narrative, Plane category, Category, Accident report] |
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