Accident Cessna 150J N60020,
ASN logo
ASN Wikibase Occurrence # 134973
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Friday 15 June 2007
Time:17:53
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150J
Owner/operator:Georges Aviation Services Inc
Registration: N60020
MSN: 150-70008
Total airframe hrs:6507 hours
Engine model:Continental O-200
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Sea near Honolulu, Oahu, HI -   United States of America
Phase: En route
Nature:Private
Departure airport:Kahului Airport, HI (OGG/PHOG)
Destination airport:Honolulu-Daniel K. Inouye International Airport, HI (HNL/PHNL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The active duty military pilot rented the airplane, while on leave, for a flight from Honolulu, Hawaii, to the island of Maui, and return. He received a checkout flight (1.2 hours) in the aircraft the day before. The pilot topped off the fuel tanks, which gave him 22.5 gallons useable, before the flight. The flight over was uneventful, but on his return flight, he lost total engine power at 2,000 feet, approximately 10 nautical miles east of his destination. The pilot described the power loss as follows: "The engine smoothly 'rolled back' in RPM to something less than cruise power as if power was simply reduced. It ran smoothly with no inconsistency for approximately one minute, and then completely stopped." He successfully ditched the aircraft into the Pacific Ocean. The two occupants exited the aircraft with an inflatable raft and were rescued. Air traffic control tower records indicate that the pilot's flight time to Maui was 1 hour, 34 minutes, and his return flight from takeoff to ditching was 45 minutes. The airplane's fuel consumption rate should have been between 6 and 7 gallons per hour. The airplane sank in deep water, and was not recovered.
Probable Cause: The total loss of engine power for an undetermined reason. A factor was the lack of suitable terrain for a forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA07CA161
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20070723X00993&key=1

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Dec-2017 18:41 ASN Update Bot Updated [Operator, Departure airport, Destination airport, Source, Narrative]
11-Jun-2023 01:31 Ron Averes Updated [[Operator, Departure airport, Destination airport, Source, Narrative]]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org