Loss of control Accident Schweizer SGS 2-32 N591CC,
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ASN Wikibase Occurrence # 137318
 
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Date:Friday 8 July 2011
Time:17:21
Type:Schweizer SGS 2-32
Owner/operator:Wave Soaring Adventures Inc
Registration: N591CC
MSN: 34
Total airframe hrs:6450 hours
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Near Ferndale Airfield - K53U, Bigfork, MT -   United States of America
Phase: En route
Nature:Training
Departure airport:Bigfork, MT (53U)
Destination airport:Bigfork, MT (53U)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot examiner reported that the purpose of the flight was to renew the pilot’s flight instructor certificate; the accident flight was the second flight of the day. Prior to the accident flight, the examiner briefed the tow plane pilot and the pilot receiving the glider check ride that the next flight would be a simulated rope break during takeoff at an altitude of about 260 feet above the ground. The examiner reported that during takeoff, he released the tow rope at 260 feet and noticed that the glider’s airspeed was slowing. He informed the pilot to increase the airspeed and bank the glider until it was lined up with runway. The examiner stated that before the glider was aligned with the runway, the pilot made a quick control stick movement to the right, which caused an accelerated stall. Multiple witnesses observed the glider depart the airport uneventfully via a tow airplane. As the glider ascended through about 200 to 300 feet, it appeared to release from the tow rope. Shortly after, the glider was observed entering a steep right bank and descended into the ground. A postaccident examination of the airframe revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
Probable Cause: The pilot’s failure to maintain adequate airspeed and his excessive control inputs during a simulated rope break while taking off, which resulted in an accelerated aerodynamic stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11LA317
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
09-Jul-2011 00:51 RobertMB Added
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 17:02 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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