ASN Wikibase Occurrence # 139515
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Date: | Friday 22 January 2010 |
Time: | 09:09 |
Type: | Bell 47G-4A |
Owner/operator: | Inland Crop Dusters Inc |
Registration: | N28938 |
MSN: | 7728 |
Year of manufacture: | 1970 |
Total airframe hrs: | 7207 hours |
Engine model: | Lycoming VO-540 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Shafter, California -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Agricultural |
Departure airport: | Shafter, CA (MIT) |
Destination airport: | Shafter, CA (MIT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he was maneuvering the helicopter to make an aerial application pass. At approximately 80 feet above ground level, he heard a muffled "crack/bang" and the helicopter immediately yawed and he experienced lateral vibrations in the cyclic. The pilot then initiated a forced landing with the shaking becoming more violent. The helicopter subsequently landed hard with the engine still running. The main rotor blades contacted and severed the tail boom, and the engine separated from its mounts. Postaccident examination of the helicopter revealed that a main rotor counterweight was missing. Examination of the broken counterweight rod end showed evidence of corrosion over approximately 45 percent of the diameter of the rod end. Maintenance records indicate that a Service Bulletin to inspect main rotor counterweight rods for pit corrosion had not been complied with. The Service Bulletin states that after an initial inspection of the main rotor counterweight rods, recurrent inspections should be accomplished every 300 hours of time in service.
Probable Cause: The loss of a main rotor blade counterweight due to corrosion. Contributing to the accident was the failure of the operator to perform the initial and recurrent inspections required by a Service Bulletin to detect the corrosion in the counterweight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA117 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
https://www.faa.gov/about/office_org/headquarters_offices/avs/offices/afs/afs700/
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
26-Oct-2011 10:16 |
Dr. John Smith |
Added |
26-Aug-2014 14:05 |
A.J.Scholten |
Updated [Cn, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 15:20 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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