ASN Wikibase Occurrence # 139550
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Date: | Thursday 27 October 2011 |
Time: | 14:40 |
Type: | Hughes 500D (369D) |
Owner/operator: | PJ Helicopters |
Registration: | N61PJ |
MSN: | 770162D |
Year of manufacture: | 1977 |
Total airframe hrs: | 11579 hours |
Engine model: | Rolls Royce C20B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Wescott Road, 6 miles W of Colusa County Airport, California -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Colusa, CA |
Destination airport: | Colusa, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The helicopter was climbing and translating away from a power and communications line tower when the engine experienced a total loss of power. At that time, the helicopter was about 175 feet above ground level and had little forward airspeed, which placed it in the portion of the height-velocity regime unfavorable for autorotation. The helicopter began to descend rapidly, the pilot began an autorotation, and the helicopter subsequently landed hard in a field.
During postaccident examination, manufacturer-specified vacuum leak checks could not determine the preimpact integrity of the fuel system due to impact damage and some initially undetected problems with the vacuum leak check equipment. About 30 gallons of fuel was found in the fuel tank, and it was free of water and other visible contaminants. Further, fuel from the fuel truck that supplied the helicopter was subsequently used in other aircraft without any problems. Detailed examinations of the airframe and engine did not reveal any mechanical deficiencies or failures that would have precluded normal operation.
Probable Cause: A total loss of engine power while maneuvering at low altitude for reasons that could not be determined because postaccident examinations did not reveal any anomalies that would have precluded normal operation. Contributing to the accident severity was the operation of the helicopter within a portion of the height-velocity regime unfavorable for autorotation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA022 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=61PJ Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2011 14:11 |
RobertMB |
Added |
28-Oct-2011 14:12 |
RobertMB |
Updated [Location, Narrative] |
23-Aug-2016 14:21 |
Dr.John Smith |
Updated [Time, Location, Departure airport, Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 17:20 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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