ASN Wikibase Occurrence # 142297
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Date: | Saturday 4 February 2012 |
Time: | 13:15 |
Type: | Piper PA-28R-201T Turbo Arrow III |
Owner/operator: | Private |
Registration: | N38906 |
MSN: | 28R-7703283 |
Year of manufacture: | 1977 |
Total airframe hrs: | 1770 hours |
Engine model: | Continental TSIO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kalispell, MT -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Kalispell, MT (KS27) |
Destination airport: | Chinook, MT (K4U4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After takeoff, between 300 and 500 feet above ground level over a residential area, the airplane's engine started to sputter and lose power. The pilot selected the longest street on which to make a forced landing, lowered the flaps, and slowed the airplane to a minimum controllable airspeed. The airplane collided with a number of vehicles and trees, and, in the process, the left wing separated from the fuselage. The airplane rotated inverted and embedded itself into the front of a residential house.
Postaccident examination and testing of the left magneto revealed that the magneto’s distributor block bushing was worn to an extent that it provided significant radial play between the bushing and distributor block. The bushing, which holds the distributor gear axle in place, would permit the distributor gear to intermittently disengage from the drive gear. Once the distributor gear had disengaged from the drive gear, the internal timing of the magneto would be off, which could disrupt the normal ignition sequence and operation of the engine. If the pilot had switched to the right magneto, engine power would have likely been restored. The most recent magneto overhaul was performed in 1989. The engine manufacturer recommends that magnetos be overhauled or replaced 5 years after the date of manufacture or last overhaul, or 4 years after the date placed in service, whichever occurs first, without regard to accumulated operating hours since new or last overhaul.
Probable Cause: The partial loss of engine power due to magneto malfunction. Contributing to the accident was the lack of adherence to the manufacturer’s recommended magneto overhaul schedule.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA092 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
05-Feb-2012 00:01 |
Alpine Flight |
Added |
06-Feb-2012 08:49 |
RobertMB |
Updated [Departure airport, Source, Narrative] |
14-Feb-2012 10:03 |
Geno |
Updated [Time, Source] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:18 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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