ASN Wikibase Occurrence # 144486
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 18 March 2012 |
Time: | 17:15 |
Type: | 2/3 scale Jenny |
Owner/operator: | Private |
Registration: | N987KB |
MSN: | 001 |
Total airframe hrs: | 2 hours |
Engine model: | Continental A-65-1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Wayne Delp Airport - 33NY, Hannacroix, NY -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | West Coxsackie, NY (33NY) |
Destination airport: | West Coxsackie, NY (33NY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The non-certificated pilot built the airplane, which was certificated about 19 months earlier. According to the pilot, the airplane had not flown, and because he wanted to ensure it was flyable again, he conducted a high-speed taxi test with no intent for flight. During the taxi test, the pilot lost control of the airplane, and by the time he had regained control, the airplane was approaching the end of the runway. To avoid the trees, the pilot decided to take off and complete one circuit to a landing. As the pilot turned the airplane onto final approach, he noted a loss of engine power. The pilot then lost control of the airplane, regained it, and attempted to land in a small field as the airplane continued to lose altitude. The pilot avoided a barn, but while doing so, the airplane hit a pine tree, spun around into the direction from which it came, and dropped nose-first to the ground. Postflight examination of the airplane revealed evidence of low power on the 65-horsepower engine at impact, and the left magneto was inoperative. Federal Aviation Administration records indicated that the pilot had previously held a student pilot certificate, which expired in 2001, and the pilot indicated that he had no flight experience in the accident airplane make and model.
Probable Cause: The non-certificated pilot's improper high-speed taxi test, which resulted in a loss of control and the pilot's subsequent decision to take off to avoid trees. Also causal, was an in-flight magneto failure, which resulted in a partial loss of engine power. Contributing to the accident was the pilot's inability to maintain control of the airplane due to his lack of total flight experience and his lack of experience in the airplane make and model.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA233 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Mar-2012 05:53 |
RobertMB |
Added |
19-Mar-2012 08:55 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Source, Narrative] |
31-Mar-2012 23:18 |
Geno |
Updated [Time, Location, Source, Narrative] |
31-Mar-2012 23:20 |
Geno |
Updated [Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:27 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation