ASN Wikibase Occurrence # 145083
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Date: | Sunday 15 April 2012 |
Time: | 17:30 |
Type: | CFM Streak Shadow |
Owner/operator: | Private |
Registration: | N2828W |
MSN: | OSS912260003 |
Total airframe hrs: | 101 hours |
Engine model: | Rotax 582 Series |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Miletus area, about 5km west of Salem, Doddridge County, WV -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Salem, WV |
Destination airport: | Salem, WV |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was attempting the first flight since the airplane was damaged in an accident about 2 years earlier and then “rebuilt.” Shortly after takeoff, the engine sputtered and lost all power. While the pilot was attempting to maneuver for a forced landing, the airplane collided with trees and terrain, resulting in substantial damage to the airframe and serious injuries to the pilot. Examination of the engine and fuel system revealed that the pistons were severely scored, indicative of a seizure. Examinations revealed that nonaviation tie wraps were used to secure the fuel lines to various fittings, and, in one location, no clamp was used. The airplane was equipped with an in-line fuel flow transducer. Disassembly of the engine revealed that the transducer incorporated a 2-millimeter (mm) jet. According to the engine manufacturer, no device with a diameter smaller than 5 mm should be installed anywhere in the fuel system. The transducer was installed on a test engine, and the engine ran normally up to 7,100 rpm with the 2-mm jet. When a small amount of air was introduced into the lines to replicate a poorly secured or unsecured fuel line, low fuel pressure and fluctuating rpm resulted, and subsequent examinations of the pistons showed signs of scoring damage.
Probable Cause: A total loss of engine power due to a piston seizure that resulted from a fuel system restriction and poorly secured fuel lines. Contributing to the accident were the pilot/builder’s failure to follow the engine manufacturer procedures and his use of nonaviation parts to secure fuel lines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA285 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
16-Apr-2012 00:49 |
gerard57 |
Added |
16-Apr-2012 03:31 |
RobertMB |
Updated [Time, Operator, Location, Source, Narrative] |
16-Apr-2012 09:49 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Source, Narrative] |
24-Apr-2012 10:04 |
Geno |
Updated [Time, Phase, Nature, Source, Damage, Narrative, Plane category, ] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:37 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Plane category] |
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