Accident Piaggio P.180 Avanti N146SL,
ASN logo
ASN Wikibase Occurrence # 147405
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 28 July 2012
Time:08:32
Type:Silhouette image of generic P180 model; specific model in this crash may look slightly different    
Piaggio P.180 Avanti
Owner/operator:Avantair Inc
Registration: N146SL
MSN: 1091
Year of manufacture:2004
Total airframe hrs:8352 hours
Engine model:P&W PT6A SER
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:San Diego, CA -   United States of America
Phase: Take off
Nature:Passenger - Non-Scheduled/charter/Air Taxi
Departure airport:San Diego, CA (KSAN)
Destination airport:Henderson, NV (KHND)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The twin-engine airplane departed 23 minutes behind schedule to pick up passengers at an intermediate airport. During the takeoff roll, the left elevator departed the airplane and was found off the side of the runway 3 days later. The crew arrived at the intermediate airport and  quickly boarded the two waiting passengers. They did not perform an adequate preflight inspection and departed about 5 minutes behind schedule. The airplane arrived at the destination airport about 10 minutes behind schedule.
Upon postflight examination by the crew, the left elevator was observed missing from the tail’s horizontal stabilizer. An examination of the attachment nuts on the hinges of the right elevator found that they were finger tight. Examination of the hinge fittings on the left elevator and horizontal stabilizer revealed no mechanical damage or deformation to any of the components. Review of airplane maintenance records showed that an airworthiness directive (AD) had been complied with 54 days earlier, which involved both elevators being removed and then reinstalled.
Materials laboratory examination of one of the right elevator attachment hardware bolt-nut combinations revealed that the self-locking nut exhibited run-on torque values well below the acceptable minimum torque. Based on the finger tight condition of the right elevator attachment hardware and the lack of any mechanical damage to the hinge fittings of the left elevator and stabilizer hinge structure, it is likely that all four sets of attachment hardware for both elevators were not properly torqued during the AD maintenance 54 days earlier. Additionally, 26 days before the event, a phase inspection was completed during which the elevator should have been visually inspected and functionally checked. The airplane had flown 158.9 hours with loose elevator attachment hardware before the two sets of bolts on the left elevator had completely worked their way out of the hinges, and the elevator departed the airplane.
The cockpit voice recorder revealed that the flight crew had experienced unusual pitch control responses during each of the departures and landings. The flight crew could have identified the missing elevator during a preflight inspection at the intermediate airport, yet they decided to continue the flight despite the pitch control problems experienced during the takeoffs and landing.

Probable Cause: The failure of maintenance personnel to properly torque the elevator attachment hardware in accordance with the maintenance manual, which led to the detachment of the elevator. Contributing to the accident were maintenance personnel’s failure to identify the loose attachment hardware during a scheduled inspection, the flight crew’s decision to continue the flight after identifying a flight control problem, and the flight crew’s failure to perform an adequate preflight inspection at the intermediate airport.

The Director of Maintenance was subsequently convicted for obstructing the NTSB investigation.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR12FA332
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB
http://aerossurance.com/safety-management/guilty-plea-obstructing-ntsb/

Location

Media:

Revision history:

Date/timeContributorUpdates
04-Aug-2012 01:02 Geno Added
07-Aug-2012 09:48 Alpine Flight Updated [Time, Aircraft type]
08-Aug-2012 23:59 Yespiaggio Updated [Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
20-Mar-2017 19:29 Aerossurance Updated [Time, Departure airport, Destination airport, Source, Narrative]
20-Mar-2017 19:32 Aerossurance Updated [Source]
27-Nov-2017 20:56 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative]
10-Mar-2021 08:24 Aerossurance Updated [Other fatalities, Source, Embed code, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org