ASN Wikibase Occurrence # 150802
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Date: | Tuesday 20 November 2012 |
Time: | 11:20 |
Type: | Cessna 210D Centurion |
Owner/operator: | Private |
Registration: | N3919Y |
MSN: | 21058419 |
Year of manufacture: | 1964 |
Total airframe hrs: | 3949 hours |
Engine model: | Continental IO-520-A (32) |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near San Rafael Airport - CA35, San Rafael, CA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | San Rafael, CA (CA35) |
Destination airport: | Chico, CA (CIC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Before departure, the pilot confirmed the fuel level by measuring the quantity of each tank, which totaled 6 gallons in the left tank and 23 gallons in the right tank. The fuel selector was placed in the right tank position for takeoff. After taking off to the northeast and when about 500 feet above ground level during the initial climb, the engine experienced a total loss of power. The pilot switched on both boost pumps, moved the fuel selector back and forth between tanks several times, and attempted to restart the engine; however, the engine did not regain power. The pilot subsequently made a forced landing to a marsh. The airplane sustained substantial damage to the lower right forward area of the fuselage, which resulted in the right fuel reservoir tank being ruptured; neither fuel tank was breached.
Recovery personnel reported that they drained 1 gallon of aviation fuel from the left fuel tank and that the fuel selector switch was in the right tank position. Postaccident examination did not reveal any anomalies that would have precluded normal operation. A postaccident test run of the engine was accomplished with no anomalies noted. After the engine run was completed, the airplane’s left and left fuel supply systems were examined. The examination revealed that there were no blockages or ruptures to the left fuel supply system and that the right fuel reservoir tank rupture permitted whatever fuel was present in the right fuel tank to drain from the system after the accident. The reason for the reported total loss of engine power could not be determined.
Probable Cause: The loss of engine power during initial climb for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR13LA047 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
21-Nov-2012 14:45 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:53 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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