ASN Wikibase Occurrence # 150838
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Date: | Wednesday 21 November 2012 |
Time: | 17:15 |
Type: | Cessna 310B |
Owner/operator: | Private |
Registration: | N5419A |
MSN: | 35619 |
Year of manufacture: | 1957 |
Total airframe hrs: | 7483 hours |
Engine model: | Continental O-470 SERIES |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | A mile into the woods north of (Rt 38) Mancelona Road in Mancelona, MI -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Mancelona, MI (4Y4) |
Destination airport: | Mancelona, MI (4Y4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A witness saw the airplane depart, however the accident was unobserved. The airplane was discovered 2 days later in a heavily wooded area about 1 mile from the departure end of the runway and about 3/4 mile to the right of the extended runway centerline. The airplane was almost inverted when it impacted the ground. Normal traffic pattern direction at the uncontrolled airport was to the left for this runway and the pilot was known to follow this requirement closely.
The accident site's location relative to the departure runway centerline and the airplane's nearly inverted attitude at impact were both consistent with the pilot's failure to maintain a minimum control airspeed and a subsequent loss of control roll to the right. The right fuel boost pump switch was found in the "on" position, whereas the left boost pump switch was found in the "off" position. Although the right fuel boost pump switch may have moved due to impact, the as-found position was consistent with the pilot attempting to correct for a loss of right engine power during takeoff.
Examination of the airframe, engine, and propeller did not reveal any anomalies associated with a preimpact failure or malfunction. N5419A cancelled Nov 2013.
Probable Cause: The pilot's failure to maintain control of the airplane after a loss of right engine power for reasons that could not be determined because postaccident examination revealed no preimpact malfunction or anomaly that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN13FA069 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB
https://www.planecrashmap.com/plane/mi/N5419A/ Location
Revision history:
Date/time | Contributor | Updates |
23-Nov-2012 12:54 |
gerard57 |
Added |
23-Nov-2012 14:14 |
Geno |
Updated [Time, Registration, Cn, Location, Departure airport, Destination airport, Source, Narrative] |
11-Jan-2013 13:37 |
Anon. |
Updated [Date, Location] |
11-Jan-2013 13:37 |
harro |
Updated [Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:53 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
02-Jul-2022 17:17 |
rvargast17 |
Updated [Location, Source, Damage, Narrative] |
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