Loss of control Accident Sikorsky S-76A N574EH,
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ASN Wikibase Occurrence # 154132
 
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Date:Friday 15 March 2013
Time:11:47
Type:Silhouette image of generic S76 model; specific model in this crash may look slightly different    
Sikorsky S-76A
Owner/operator:Era Helicopters Llc
Registration: N574EH
MSN: 760369
Year of manufacture:1990
Total airframe hrs:6760 hours
Engine model:Turbomeca ARRIEL 1S1
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Grand Lake, LA -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Lake Charles, LA (KLCH)
Destination airport:Lake Charles, LA (KLCH)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot and two mechanics were conducting a post-maintenance check flight of the helicopter’s avionics system. After testing the avionics, the pilot allowed the mechanic to fly the helicopter at 1,000 feet above ground level. The mechanic maneuvered the helicopter for about 1 minute and then stated that he was transferring control of the helicopter back to the pilot. Two seconds later, the cockpit voice recorder (CVR) cut off. About 1 minute after the CVR cut off, the pilot made a routine radio call to the tower controller that he was returning to land. Two minutes after this call, the pilot radioed the tower controller and his company’s dispatcher, stating that he had a problem and would be landing off-airport immediately. Several ground witnesses noticed the helicopter as it flew toward the accident site, and it was making an unusual noise, described as grinding, screeching, or whistling. The helicopter impacted with a high vertical descent rate and a postcrash fire ensued.
Examination of the helicopter revealed that the main rotor and tail rotor systems had low rotational energy at the time of ground impact. Two of the tail rotor blades (yellow and red) were fractured adjacent to the tail rotor hub. The fracture signatures on the red/yellow tail rotor spar assembly were consistent with the red tail rotor blade spar initially fracturing and the red tail rotor blade departing from the tail rotor.
The resultant imbalance of the tail rotor fractured the tail gearbox (TGB) output housing studs and most likely tripped the CVR g-switch, which cut off the CVR. The yellow tail rotor blade spar fractured due to high centrifugal forces as a result of the imbalance, and the yellow blade departed from the tail rotor; the tail rotor was then rebalanced. The two remaining tail rotor blades continued to provide partial tail rotor anti-torque, and tail rotor drive remained continuous through the TGB. The entirety of the red and yellow blade separation event likely occurred very quickly, with only a momentary bump or vibration at the time of blade separation.  
As the TGB output housing began to separate from the center housing, the gears likely began going out of mesh, allowing the output bevel gear to eventually contact the TGB center housing. This condition likely resulted in the loud, unusual noise reported by witnesses, as well as a drag force on the tail rotor drive system. As the pilot attempted to land, he likely shut the engines down in conjunction with an autorotative landing. Because the tail rotor drive system and main transmission remained mechanically linked, when the engines were shut down, it is likely that main rotor speed (Nr) degraded due to the compromised TGB. As a result, the helicopter developed a high vertical descent rate until ground impact.
The red blade spar fracture signatures were consistent with a fast-growth failure mode. Plausible fast-growth failure modes that were examined included a discrete impact event (e.g. object strike), anomalous operation of the pivot bearing, and a fracture of the pitch horn box (the structure which attaches the pitch horn to the blade and to which the pivot bearings and bumper attaches). With the lack of available evidence because the red blade was not recovered, the specific failure mode could not be determined during the investigation.   


Probable Cause: Fracture of the red tail rotor blade spar, which resulted in the separation and departure of the red tail rotor blade from the helicopter and subsequent compromised tail gearbox. The red tail rotor blade was not recovered, thus the cause of the initial fracture could not be determined.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN13FA192
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=574EH

Location

Revision history:

Date/timeContributorUpdates
16-Mar-2013 02:59 gerard57 Added
16-Mar-2013 06:43 krasatpi Updated [Cn]
17-Mar-2013 01:48 RobertMB Updated [Time, Aircraft type]
17-Mar-2013 06:49 Geno Updated [Departure airport, Destination airport, Source]
27-Aug-2013 19:21 Anon. Updated [Aircraft type]
04-Feb-2015 21:47 Aerossurance Updated [Location, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
28-Nov-2017 14:15 ASN Update Bot Updated [Aircraft type, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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