ASN Wikibase Occurrence # 157102
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 29 November 1999 |
Time: | 15:05 LT |
Type: | Cessna 152 |
Owner/operator: | The Global Group Inc. |
Registration: | N48WT |
MSN: | 15283366 |
Year of manufacture: | 1979 |
Total airframe hrs: | 9510 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Open field in Surprise, 15 miles NW of Glendale, AZ -
United States of America
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | Glendale, AZ (KGEU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot is chief pilot for a flight school, and reported that a renter pilot had made an emergency landing in a cow pasture in the accident airplane after running out of fuel. The airplane sat in the field unattended over the weekend. The pilot and one of the school's mechanics assessed the damage; none was found. The pilot planned to transport the airplane back to the airport. He put in fuel and performed a preflight and control check with no noted discrepancies. The pilot and the mechanic then moved the airplane to a rough dirt road; the pilot measured the available takeoff distance about 1,500 feet. He reported that the takeoff and initial climb out seemed normal, but the airplane then started turning left. The pilot applied right rudder and aileron but was not able to stop the turn. His airspeed was in the 50-knot range, but about 35 to 40 feet agl, the airplane began to settle while still in an 18- to 20-degree left bank. The stall warning indicator did not activate at any time. The left wing tip impacted the ground, followed by the nose of the airplane. The airplane nosed over and came to rest inverted. The pilot stated that the winds alternated from calm to light and variable at 1 to 2 knots at the time of the accident. A postcrash examination revealed that the flaps, ailerons, and rudders operated normally. No mechanical discrepancies were found with any airframe or engine system.
Probable Cause: The pilot's failure to attain and maintain an adequate airspeed during takeoff from a short and unimproved dirt road, which resulted in an inadvertent stall/mush condition and impact with the ground.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00LA044 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX00LA044
Location
Revision history:
Date/time | Contributor | Updates |
25-Jun-2013 10:35 |
JINX |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:47 |
ASN Update Bot |
Updated [Cn, Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 16:38 |
ASN Update Bot |
Updated [Time, Other fatalities, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation