ASN Wikibase Occurrence # 157124
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Date: | Thursday 2 December 1999 |
Time: | 12:24 LT |
Type: | Piper PA-28-181 |
Owner/operator: | West Valley Flying Club |
Registration: | N4319Y |
MSN: | 28-8490010 |
Year of manufacture: | 1983 |
Total airframe hrs: | 5698 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Palo Alto Airport, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Carlsbad, CA (KCRQ) |
Destination airport: | (KPAO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Prior to departure to return to home base, the pilot filed an IFR flight plan, conducted a preflight, and had the fuel tanks topped off. He flew on the left fuel tank for approximately 1 hour and then switched to the right fuel tank. Upon reaching his destination he noted multiple cloud layers, and requested and received an IFR clearance to his destination airport. About an hour later he switched back to the left fuel tank. He noted a drop to zero in the left fuel gage about 45 minutes later, and switched to the right tank, where he noted that the fuel gage read 5 gallons. He switched back to the left tank and the engine stopped; he switched back to the right tank and the engine restarted. He declared minimum fuel and received information on nearby airports; one 7 miles in his direction of flight, and his destination airport was 11 miles in his direction of flight. He continued the flight to the destination airport in order to lose altitude. He was at 4,000 feet, and traffic pattern altitude is 800 feet. He requested a straight in to a runway 30 even though 12 was the active runway. On short final, he initiated a go-around due to high speed, and high altitude. During the turn back to the runway the engine lost power and landed in a marshy area. There was no fuel observed in the tanks during the recovery of the airplane. During the engine examination it was noted that were was no fuel staining observed on the wings or fuselage of the airplane, and there were no leaks in the fuel system. No discrepancies were noted with the run-up.
Probable Cause: The failure of the pilot to properly calculate fuel consumption rate, and his improper in-flight planning to continue the flight to the destination airport instead of landing at a closer alternate airport. A factor was the pilot's inadequate aircraft control during the descent, which necessitated a go-around.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00LA067 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX00LA067
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
25-Jun-2013 15:46 |
JINX |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:59 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
07-Apr-2024 16:37 |
ASN Update Bot |
Updated [Time, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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