ASN Wikibase Occurrence # 157262
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Date: | Tuesday 25 June 2013 |
Time: | 08:25 |
Type: | Mooney M20J 201 |
Owner/operator: | Private |
Registration: | N205MC |
MSN: | 24-3012 |
Total airframe hrs: | 2600 hours |
Engine model: | Lycoming IO-360-A3B6D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Route 66, west of El Reno, OK -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Bethany, OK (PWA) |
Destination airport: | Bethany, OK (PWA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the engine abruptly lost power while he was practicing instrument approaches under visual flight rules. His efforts to restore engine power were unsuccessful. The pilot subsequently executed a forced landing to the center median of a roadway. A postaccident examination revealed that the dual magneto assembly was not functioning properly. Although the magneto drive shaft operated during engine crankshaft rotation, the magneto points did not open as required. A teardown examination revealed that the magneto components were worn. In addition, the threaded inserts had lifted out of the mounting block. The magneto assembly was inspected less than 1 flight hour before the accident during an engine propeller strike inspection, and the magneto block, points, and cam were replaced at that time. The accident flight was the second flight since the inspection and maintenance work had been performed. Although the magneto points might have been misaligned due to the threaded insert lifting out of the mounting block, it is unlikely that such a discrepancy would have resulted in a loss of magneto function within such a short timeframe. The magneto failure caused the loss of engine power; however, the cause of the magneto failure could not be determined.
Probable Cause: A loss of engine power, which resulted from the failure of the magneto assembly for reasons that could not be determined during postaccident examinations.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN13LA370 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
27-Jun-2013 03:20 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 08:46 |
ASN Update Bot |
Updated [Operator, Nature, Departure airport, Destination airport, Source, Narrative] |
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