ASN Wikibase Occurrence # 158023
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Date: | Friday 2 August 2013 |
Time: | 09:40 |
Type: | Mooney M20F Executive 21 |
Owner/operator: | Private |
Registration: | N2926M |
MSN: | 22-1282 |
Year of manufacture: | 1975 |
Engine model: | Lycoming IO360 SER A&C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Helena Regional Airport (KHLN), Helena, MT -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Helena, MT (HLN) |
Destination airport: | Helena, MT (HLN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor reported that the purpose of the flight was for the pilot-undergoing instruction to perform touch-and-go practice takeoffs and landings. During the approach, the airplane was slightly fast and touched down about halfway down the runway. The instructor thought the pilot could still successfully complete a takeoff and monitored him as he retracted the flaps. As the airplane continued down the runway, the instructor decided that the airplane’s climb performance would not be sufficient to clear obstacles at the end of the runway and he opted to abort the takeoff. The instructor retarded the throttle lever to the closed position and told the pilot to apply maximum braking pressure. The airplane subsequently went off the end of runway into a grass field and continued about 100 feet before impacting a chain-link fence. During the accident sequence, the wing spar was substantially damaged.
The airplane’s brake pedals were only accessible to the left-seated person, which is where the pilot was positioned. The instructor reported no mechanical malfunctions or failures with the airplane that would have precluded normal operation. He additionally stated that this accident could have been prevented by making a timely decision to go-around when it was apparent that the airplane was going to touchdown further down the runway.
Probable Cause: The flight instructor's delayed decision to instruct the pilot to abort the landing which resulted in a runway excursion and collision with a fence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR13CA355 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N2926M Location
Revision history:
Date/time | Contributor | Updates |
05-Aug-2013 22:34 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:00 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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