ASN Wikibase Occurrence # 165211
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Date: | Thursday 20 March 2014 |
Time: | 12:05 |
Type: | Cessna 421B Golden Eagle |
Owner/operator: | Private |
Registration: | N5929M |
MSN: | 421B0312 |
Year of manufacture: | 1972 |
Total airframe hrs: | 6660 hours |
Engine model: | Continental GTSIO-520-C |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Charleston AFB/Int'l Airport (KCHS), Charleston, SC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Columbia, SC (CUB) |
Destination airport: | Charleston, SC (CHS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was concluding a personal flight with two passengers on board. The pilot reported that, during the landing roll and after a normal touchdown on the concrete runway, the right main landing gear (MLG) collapsed. The airplane then veered right and struck two runway lights, which resulted in substantial damage to the right wing rear spar.
Examination of the airplane revealed that the right MLG down-lock bellcrank was fractured and had separated from its respective trunnion. The bellcrank bolt was sheared at the bolt head, consistent with overload. The upper end of the bellcrank remained attached to the outboard push-pull tube. The lower end of the bellcrank, which attached to the rod end fitting at the lower side link, was broken, consistent with a ductile tension failure. The fracture location was consistent with additional stress that would have been placed on the bellcrank if the landing gear was not properly rigged; however, damage to the landing gear precluded the ability to functionally check or verify whether the gear was properly rigged. Review of maintenance records revealed that the airplane had been operated for about 4 hours since its most recent annual inspection, which was performed about 2 months before the accident. At that time, maintenance, including the adjustment of the right MLG travel, was performed on the airplane.
Probable Cause: Inadequate maintenance, which resulted in the collapse of the right main landing gear during landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA170 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N5929M FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N5929M Location
Revision history:
Date/time | Contributor | Updates |
03-Apr-2014 22:42 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 13:47 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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