ASN Wikibase Occurrence # 165948
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 13 April 2014 |
Time: | 15:42 |
Type: | LET L-33 Blanik Solo |
Owner/operator: | North Carolina Soaring Association |
Registration: | N318BA |
MSN: | 970418 |
Year of manufacture: | 1997 |
Total airframe hrs: | 592 hours |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | NNE of Crooked Creek Airport (7NC5), Bunn, North Carolina -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Bunn, NC (7NC5) |
Destination airport: | Bunn, NC (7NC5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The glider was towed aloft and then released. Shortly after, the glider pilot radioed the towplane pilot and informed him that he was returning to the airport. Because of the short duration of the glider flight, the towplane pilot asked the glider pilot if he wanted to be towed aloft again, and he replied that he did. Witnesses on the ground reported observing the glider low on the downwind leg and then turning onto the base leg. Based on data from the onboard portable GPS receiver, the glider turned onto final approach and flew in a southerly direction toward the runway with its groundspeed decreasing from 34 to 25 knots during the last few seconds of the flight. The glider impacted the ground in a nose-low attitude, which caused the wing to separate.
Postaccident examination of the glider found no evidence of a preimpact failure or malfunction of the flight controls or air brakes, and the air brakes were retracted. The published stall speed for the glider with the air brakes retracted is about 34 knots indicated airspeed. Although the indicated airspeed during the final portion of the flight could not be determined, the evidence indicates that the pilot likely failed to maintain adequate airspeed while approaching the airport, which resulted in a stall/mush.
Probable Cause: The pilot’s failure to maintain airspeed while approaching the airport, which resulted in a stall/mush.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA199 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=318BA Location
Revision history:
Date/time | Contributor | Updates |
02-May-2014 23:49 |
Geno |
Added |
14-May-2014 20:19 |
Alpine Flight |
Updated [Aircraft type] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 14:02 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
01-Apr-2022 19:04 |
Ron Averes |
Updated [Aircraft type, Source] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation