ASN Wikibase Occurrence # 170955
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Date: | Sunday 2 November 2014 |
Time: | 14:56 |
Type: | Cessna T210M Turbo Centurion |
Owner/operator: | Private |
Registration: | N1593M |
MSN: | 21061949 |
Year of manufacture: | 1977 |
Total airframe hrs: | 5308 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Applegate Valley, SW of Jacksonville, OR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Grants Pass, OR |
Destination airport: | Long Beach, CA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during cruise flight, the engine began running roughly with smoke developing inside the cabin, followed by oil covering the windshield. The pilot stated that the engine continued to run and that his attempts to increase the power setting resulted in severe shaking and more smoke. The pilot initiated a forced landing in a nearby field. During the landing roll, the nosewheel landing gear dug into mud, and the airplane subsequently nosed over.
Postaccident examination of the engine revealed that the Nos. 5 and 6 connecting rods were liberated from the crankshaft. The No. 6 connecting rod was thermally discolored and fractured, which was likely caused by oil starvation to the No. 6 connecting rod journal and bearing. The No. 5 connecting rod was also fractured; however, the connecting rod and bearing did not exhibit thermal discoloration or distress; the fracture likely resulted due to damage sustained when the No. 6 connecting rod fractured. The Nos. 1 and 2 connecting rods also exhibited thermal discoloration and distress, which likely resulted from the engine’s continued operation after the liberation of the No. 6 connecting rod.
Probable Cause: A loss of engine power during cruise flight due to the failure of the No. 6 connecting rod, which resulted from oil starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15LA032 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N1593M/history/20141102/2200Z/3S8/KMFR FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=1593M Location
Revision history:
Date/time | Contributor | Updates |
03-Nov-2014 04:04 |
Geno |
Added |
03-Nov-2014 04:05 |
Geno |
Updated [Aircraft type] |
12-Nov-2014 01:22 |
Geno |
Updated [Nature, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:34 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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