ASN Wikibase Occurrence # 171484
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Date: | Friday 21 November 2014 |
Time: | 10:00 |
Type: | Piper PA-24-250 Comanche |
Owner/operator: | Private |
Registration: | N7428P |
MSN: | 24-2616 |
Year of manufacture: | 1961 |
Total airframe hrs: | 4932 hours |
Engine model: | Lycoming O-540-A1D5 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | SW of Garberville Airport (O16), Garberville, CA -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Cameron Park, CA (O61) |
Destination airport: | Garberville, CA (O16) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was conducting a routine cross-country flight to the destination airport. The pilot had conducted this same flight once a month for the previous 5 years to serve as a community rural doctor. Numerous witnesses reported observing the airplane maneuvering toward the airport at a very low altitude just below the cloud layer. Several witnesses near the accident site stated that they did not hear any engine noise. The airplane impacted a tree about 2,260 ft short of the approach end of the runway and came to rest in a river, partially resting on a gravel/sand embankment. Following the accident, the water level quickly rose, nearly submerging the entire airframe.
Although a postaccident examination revealed no evidence of preimpact mechanical malfunctions or failures, the extent of the damage sustained during the collision and the water immersion precluded a detailed determination of the engine and fuel system preimpact condition, settings, and functionality. One of the three propeller blades was bent aft about 80 degrees near the blade root, but the other two blades were undamaged. Based on this minimal damage and the witnesses’ accounts of not hearing engine noise, it is likely that the engine experienced a loss of power while the pilot was on approach to the airport.
Fuel was found in the fuel lines forward of the firewall; therefore, it is unlikely that fuel exhaustion or starvation occurred. The fuel mixture cable was found disconnected from the mixture arm on the carburetor. Given the minimal damage to the mixture arm and that it was not spring-loaded to any position, it is possible that the cable became disconnected in flight and adversely affected the engine operation. However, there was insufficient evidence to determine when the cable became disconnected or whether or when it affected the engine operation.
Probable Cause: A loss of engine power for reasons that could not be determined due to extensive damage sustained during the collision and postaccident water immersion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15FA045 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N7428P Location
Revision history:
Date/time | Contributor | Updates |
21-Nov-2014 23:16 |
Geno |
Added |
25-Nov-2014 06:05 |
Geno |
Updated [Time, Phase, Nature, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:34 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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