ASN Wikibase Occurrence # 173342
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Date: | Friday 9 January 2015 |
Time: | 11:00 |
Type: | Cessna 150G |
Owner/operator: | Griffith Aviation Inc |
Registration: | N2871S |
MSN: | 15066771 |
Year of manufacture: | 1967 |
Total airframe hrs: | 7409 hours |
Engine model: | Continental O-200 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Pontiac Municipal Airport (KPNT), Pontiac, IL -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Griffith, IN (05C) |
Destination airport: | Pontiac, IL (PNT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the flight instructor, the student pilot was attempting to land the airplane but conducted an attempted go-around. The flight instructor then took control of the airplane. The student pilot reported that, as the flight instructor was attempting the second landing, the airplane bounced, at which time, the flight instructor initiated a go-around. The flight instructor reported that the engine then began to sputter and that, when he turned off the carburetor heat, the engine quit as the airplane was about 5 ft above the ground. He further stated that a right crosswind pushed the airplane to the left and that he subsequently attempted to land the airplane in a field left of the runway; however, the landing gear sunk into the snow, and the airplane subsequently nosed over. Examination of the airplane, engine, and carburetor revealed no anomalies. The reason for the loss of engine power could not be determined. Based on the available information, it is likely that the flight instructor lost directional control during the attempted go-around, which resulted in an off-runway landing and a subsequent nose-over.
Probable Cause: The flight instructor’s loss of directional control during an attempted go-around with a crosswind. Contributing to the accident was the loss of engine power for reasons that could not be determined during examination of the engine.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA114 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=2871S Location
Revision history:
Date/time | Contributor | Updates |
27-Jan-2015 23:21 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 11:49 |
ASN Update Bot |
Updated [Total occupants, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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