ASN Wikibase Occurrence # 174994
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Date: | Friday 4 July 1997 |
Time: | 11:25 |
Type: | Quickie Q200 |
Owner/operator: | Private |
Registration: | G-BUOO |
MSN: | 01 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Cranfield, Bedfordshire -
United Kingdom
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Coventry-Baginton Airport (CVT/EGBE) |
Destination airport: | Cranfield, Bedfordshire (EGTC) |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Written off (destroyed) 4 July 1997 when crashed on landing and caught fire at Cranfield, Bedfordshire. According to the following extract from the official AAIB report into the accident:
"The pilot had flown from Coventry to Cranfield, in order to attend a "Fly In". The weather at Cranfield was benign with no significant weather or cloud, and a surface wind of 330 degrees/06 knots.
Runway 22 was in use, it has an asphalt surface and an available landing distance of 1,680 metres, the runway surface was dry. The pilot had made three unsuccessful approaches to land before commencing the final approach, he had been concerned that traffic ahead of him might restrict his use of the runway, and he wanted to ensure that control of the speed and approach profile were correct.
A video recording shows that a normal landing was made from the fourth approach, after which the aircraft immediately commenced a pilot induced oscillation in pitch. After four bounces between the main wheels and the nose wheel, the pilot applied some power, and the aircraft accelerated slowly, before getting airborne after three further substantial oscillations between the main wheels and the nose wheel.
The aircraft then flew for a further one hundred metres or so, before landing once again, but now out of the view of the video camera. After this second landing, the pilot stated that the aircraft pitched forward once again, the nose wheel oleo then collapsed, followed by a loud bang, as the propeller struck the runway surface and splintered.
A fire soon developed as the aircraft slid to a halt, leaving a trail of burning fuel in its wake; both occupants immediately vacated the aircraft without assistance. The airfield fire and rescue services were quickly on the scene, and extinguished the fire. The pilot was subsequently taken to hospital with serious burns to his arm, the passenger was uninjured".
The AAIB report confirms that the aircraft was "destroyed"; as a result, the registration G-BUOO was belatedly cancelled by the CAA on 6 June 2001
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
1. AAIB:
https://www.gov.uk/aaib-reports/quickie-tri-q-200-g-buoo-4-july-1997 2. CAA:
http://www.caa.co.uk/aircraft-registration/ 3.
http://www.quickheads.com/index.php?option=com_content&view=article&id=1567:q-accident-reports&catid=58:safety&Itemid=181 Revision history:
Date/time | Contributor | Updates |
31-Mar-2015 19:58 |
Dr. John Smith |
Added |
31-Mar-2015 20:01 |
Dr. John Smith |
Updated [Narrative] |
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