ASN Wikibase Occurrence # 175980
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Date: | Thursday 7 May 2015 |
Time: | 17:50 |
Type: | Bell UH-1B |
Owner/operator: | R |
Registration: | N46969 |
MSN: | 63-8548 |
Year of manufacture: | 1963 |
Total airframe hrs: | 24111 hours |
Engine model: | Lycoming T53 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Pierre Lake, Orient, Washington -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | External load operation |
Departure airport: | Kettle Falls, WA |
Destination airport: | Kettle Falls, WA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was conducting an external load logging flight in the helicopter. A review of maintenance records revealed that, on the day of the accident, the engine had been replaced with an overhauled engine. Following the maintenance, the pilot completed one logging cycle without incident. The pilot reported that, about 50 minutes into the second cycle, she heard a loud screeching/grinding noise followed by a muffled “bang.” The low rotor rpm horn sounded, and she initiated an autorotation. The helicopter touched down, impacted trees, rolled down sloped terrain, and then came to rest.
A postaccident examination of the engine’s particle separator assembly revealed that it was intact and installed properly on the air inlet section; however, the inlet guide vanes exhibited signatures consistent with foreign object damage, and a material consistent with a towel was found within the vanes. Given the damage signatures and the found material, it is likely that maintenance personnel did not adequately inspect the engine area after installing the overhauled engine and left a towel in its compressor section, which the engine subsequently ingested and resulted in a total loss of power.
Probable Cause: A total loss of engine power due to foreign object (towel) ingestion. Contributing to the accident was maintenance personnel’s inadequate postmaintenance inspection of the engine.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15LA159 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=46969
History of this aircraft
Other occurrences involving this aircraft
5 December 2007 |
N46969 |
R AND R Conner Aviation |
0 |
33 miles SW of Ennis, MT |
|
sub |
Bounced on landing |
Location
Revision history:
Date/time | Contributor | Updates |
08-May-2015 06:42 |
Iceman 29 |
Added |
08-May-2015 06:43 |
harro |
Updated [Aircraft type, Total fatalities, Total occupants, Other fatalities, Location, Source, Damage, Narrative] |
08-May-2015 16:52 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Location, Phase, Nature, Source, Damage, Narrative] |
07-Jun-2015 08:54 |
stevethehumbersider |
Updated [Cn, Narrative] |
26-Jul-2015 16:42 |
Anon. |
Updated [Narrative] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 13:07 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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