Accident Piper PA-24-250 Commanche N6168P,
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ASN Wikibase Occurrence # 177468
 
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Date:Wednesday 1 July 2015
Time:13:54
Type:Silhouette image of generic PA24 model; specific model in this crash may look slightly different    
Piper PA-24-250 Commanche
Owner/operator:Private
Registration: N6168P
MSN: 24-1269
Year of manufacture:1959
Engine model:Lycoming O-540-A1A5
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Near Rockin M Airport (T14), Quinlan, TX -   United States of America
Phase: Take off
Nature:Private
Departure airport:Quinlan, TX (T14)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane, which was owned and operated by the private pilot, experienced a total loss of engine power shortly after takeoff, descended, and impacted a field. A fire erupted that consumed the majority of the airplane's cabin and the inboard sections of both wings. The wreckage distribution, ground scars, and crushing of the wing leading edges were indicative of a low-speed nose-down impact and consistent with an aerodynamic stall. Examination of the fuel system revealed the presence of rust and water in both electric fuel pumps and water in the engine carburetor bowl. The examination revealed no other engine or airframe anomalies that would have precluded normal operation. The rust found in the fuel pumps indicated that the fuel system had been contaminated with water for a long period of time. The airplane owner's handbook provided clear and explicit instructions on how to check before flight for fuel system contamination.
Probable Cause: The pilot's failure to maintain control of the airplane following a loss of engine power during initial climb after takeoff, which resulted in the wing's critical angle-of-attack being exceeded and a subsequent aerodynamic stall. Also causal was the pilot's inadequate preflight inspection of the airplane's fuel system, which resulted in the loss of engine power due to water contamination.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN15FA287
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
01-Jul-2015 20:07 Geno Added
01-Jul-2015 20:20 Geno Updated [Time, Aircraft type, Registration, Cn, Operator, Location, Source]
01-Jul-2015 21:01 Geno Updated [Source]
09-Jul-2015 18:11 Geno Updated [Time, Nature, Source]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
01-Dec-2017 15:03 ASN Update Bot Updated [Other fatalities, Departure airport, Source, Narrative]

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