Accident Bellanca 7KCAB N4173Y,
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ASN Wikibase Occurrence # 177722
 
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Date:Wednesday 26 May 2004
Time:17:20
Type:Silhouette image of generic CH7B model; specific model in this crash may look slightly different    
Bellanca 7KCAB
Owner/operator:Private
Registration: N4173Y
MSN: 598-077
Total airframe hrs:5743 hours
Engine model:Lycoming IO-320-E2D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Peyton, CO -   United States of America
Phase: Landing
Nature:Private
Departure airport:Peyton, CO (00V)
Destination airport:Peyton, CO (00V)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, as he returned to Meadow Lake, he received weather conditions from the local Automated Surface Observing System (ASOS). ASOS reported winds from 250 degrees at 13 knots, gusting to 17 knots. The pilot decided to "attempt a landing." While on final approach for runway 33, the pilot noticed that his rate of descent had increased to approximately 1000 feet per minute. The pilot added engine power, and increased the airplane's angle of attack and bank, to compensate for the crosswind conditions. The pilot said that during the flare, the airplane "floated" and he had to fly at an "unsafe bank angle...to maintain [runway] centerline." The pilot decided to abort the landing and added full power for a go-around. The pilot said, at approximately 10 to 25 feet above the ground, a gust of wind struck the airplane and although he was not able to maintain runway centerline, the airplane "seemed to be controllable." The pilot said he was unable to maintain level flight and the airplane continued to drift to the right of the runway centerline. When he entered a 20 to 30 degree right bank to avoid some trees, the airplane's right wing struck the ground. The airplane cart wheeled several times causing substantial damage to the airplane's fuselage, wings, and empennage.
Probable Cause: the pilot's inadequate in-flight planning and decision making and his failure to maintain aircraft control during the landing flare which resulted in impact with terrain. Contributing factors include the pilot's failure to perform a go-around and the wind gust.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN04LA081
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040616X00803&key=1

Revision history:

Date/timeContributorUpdates
11-Jul-2015 16:58 Noro Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:01 ASN Update Bot Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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