Accident Hughes 269C N56PH,
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ASN Wikibase Occurrence # 180006
 
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Date:Friday 9 July 2004
Time:20:10
Type:Silhouette image of generic H269 model; specific model in this crash may look slightly different    
Hughes 269C
Owner/operator:Private
Registration: N56PH
MSN: S-1441
Engine model:Lycoming HIO-360-D1A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:about 12 miles north of Arlington, Washington -   United States of America
Phase: Landing
Nature:Private
Departure airport:Bellingham, WA (BLI)
Destination airport:Arlington, WA (AWO)
Investigating agency: NTSB
Confidence Rating: Information verified through data from accident investigation authorities
Narrative:
While cruising at about 2,500 feet above the ground (agl), the pilot heard a "pop" and felt the helicopter yaw to the right. Almost immediately he noticed that the engine was starting to lose power, and he therefore lowered the collective and initiated a partial autorotation. He then attempted to get the engine to accelerate, but he continued to hear "sputtering and popping," and the engine continued to gradually lose power. The pilot therefore elected to perform a full autorotational landing in a nearby opening in the heavily wooded area he was flying over. Although he was able to touch down with only a very slow forward speed, the terrain he was landing on turned out to be a wet and muddy bog or swamp, and as the helicopter touched down, one of the skids sunk into the mud, and the aircraft rolled over onto its side. A post-accident inspection of the helicopter's engine and fuel system by an FAA Airworthiness Inspector and a fixed base operator's (FBO's) maintenance personnel did not find any evidence of an anomaly that would have lead to a loss of power in the engine. After the initial inspection was completed, the engine was mounted on an engine stand and run at various speeds for a period of about eight minutes. During the test run, the engine started easily and ran smooth at all tested speeds up to and including a maximum of 3,100 rpm.




Probable Cause: A significant power loss for undetermined reasons while in cruise flight, leading to a full autorotational landing. Factors include no suitable terrain in the area, and soft swampy terrain at the point where the pilot found it necessary to perform the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA04LA128
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040722X01031&key=1

Location

Revision history:

Date/timeContributorUpdates
29-Sep-2015 13:58 Noro Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:12 ASN Update Bot Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative]
21-Sep-2019 14:53 BEAVERSPOTTER Updated [Cn]

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