Accident Piper PA-28R-200 Arrow N9336N,
ASN logo
ASN Wikibase Occurrence # 188281
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 19 June 2016
Time:20:45
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-200 Arrow
Owner/operator:Private
Registration: N9336N
MSN: 28R-35036
Year of manufacture:1969
Engine model:Lycoming IO360
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Bowie Municipal Airport (0F2), Bowie, TX -   United States of America
Phase: Landing
Nature:Private
Departure airport:Omaha, NE (KOMA)
Destination airport:Bowie, TX (0F2)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot reported that he had just completed a cross-country flight and had been cleared for the approach when, during the descent, the engine did not respond when he pulled back on the throttle. When the pilot enriched the fuel/air mixture, the manifold pressure decreased, and the engine lost power. The pilot conducted a forced landing to a field, during which the airplane’s wing sustained substantial damaged.
The examination of the engine revealed that the throttle control arm, which was original hardware to the airplane, was separated from the joint assembly. Additionally, the female end of the throttle arm exhibited elongation at the linkage attachment point and was consistent with wear developing over time. An examination of the airplane, engine, and remaining systems revealed no other anomalies that would have precluded normal operation.
The airplane manufacturer had issued a nonmandatory service letter (SL) recommending that the throttle arm and joint assembly be replaced with a new refinement kit if any indication of wear existed; a review of the engine logbooks found no record of compliance with the SL. Although the pilot reported that the airplane’s last inspection was an annual inspection, he did not provide the date of the inspection, and it was not noted in the logbook. Given the condition of the throttle linkage attachment, it is likely that the inspection of the throttle linkage attachment was either not performed or was inadequate. Investigators were unable to determine what the exact state of the throttle arm was at the last inspection.

Probable Cause: The inadequate maintenance and inspection of the throttle control arm, which resulted in its in-flight separation and the subsequent loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN16LA227
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
https://flightaware.com/live/flight/N9336N

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?nNumberTxt=9336N

Location

Revision history:

Date/timeContributorUpdates
20-Jun-2016 22:04 Geno Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
19-Aug-2017 14:56 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org