ASN Wikibase Occurrence # 189699
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Date: | Sunday 6 August 2006 |
Time: | 14:45 |
Type: | Denney Kitfox 3 |
Owner/operator: | Private |
Registration: | G-BTMX |
MSN: | PFA172-12079 |
Year of manufacture: | 1993 |
Engine model: | Rotax 582 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Near Wheaton Ashton, Staffordshire -
United Kingdom
|
Phase: | En route |
Nature: | Private |
Departure airport: | Otherton Airfield, Micklewood Lane, Penkridge, Staffordshire |
Destination airport: | Otherton Airfield, Micklewood Lane, Penkridge, Staffordshire |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Written off (damaged beyond repair) 06-08-2006 when crashed near Wheaton Aston, Staffordshire (at approximate co ordinates 52°43′56″N, 02°14′05″W). The two persons on board (pilot and one passenger) sustained severe spinal and other injuries. According to the following excerpt from the official AAIB report into the accident:
"The aircraft was a few minutes into a short local flight and was returning to Otherton. Due to the short distance of the intended flight, the pilot decided to cruise at 1,000 feet amgl. During the flight the engine suddenly stopped and the pilot was unaware of any warning of engine failure.
The pilot selected a field and commenced a downwind leg for an approach. His passenger noticed some cables in the selected field and notified the pilot. The pilot was unable to see the cables but was conscious of the aircraft’s lack of height, and quickly selected another field slightly further downwind.
This field appeared, from pictures taken by the Police Air Support Unit after the accident, to be suitable in both size and surface condition for a forced landing. However, on final approach the aircraft was too low to reach the intended
field and landed approximately 80 m short in another large field containing a three to four foot high cereal crop.
During the landing the aircraft slewed round through 180 degrees and decelerated rapidly. The pilot crawled out of the aircraft through a door and called the emergency services using a mobile phone. Both occupants, who had been wearing full harnesses, were airlifted to hospital suffering from spinal fractures and other injuries".
Damage sustained to airframe: Per the AAIB report "Although the aircraft was upright and largely intact, there was damage to the propeller, left wing leading edge, both landing gear legs, the underside of the fuselage, and significant damage to the rear fuselage. As a result the aircraft was written off". As a result, the registration G-BTWX was cancelled by the CAA on 26-01-2007 as "Destroyed"
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | EW/G2006/08/05 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
1. AAIB:
https://assets.publishing.service.gov.uk/media/5422f075e5274a131700030f/Denney_Kitfox_Mk_3__G-BTMX_04-07.pdf 2. CAA:
https://siteapps.caa.co.uk/g-info/rk=BTMX 3.
http://www.airport-data.com/aircraft/photo/000030393.html Revision history:
Date/time | Contributor | Updates |
30-Aug-2016 23:32 |
Dr.John Smith |
Added |
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