ASN Wikibase Occurrence # 191266
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Date: | Thursday 10 November 2016 |
Time: | 09:15 LT |
Type: | North American Navion A |
Owner/operator: | Private |
Registration: | N8849H |
MSN: | NAV-4-849 |
Year of manufacture: | 1947 |
Total airframe hrs: | 2066 hours |
Engine model: | Continental IO-520-BB |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Blairstown Airport (1N7), Blairstown, NJ -
United States of America
|
Phase: | Taxi |
Nature: | Ferry/positioning |
Departure airport: | Blairstown, NJ (1N7) |
Destination airport: | Harrisburg, PA (CXY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot had not flown the accident airplane for almost 1 year while it underwent repairs following a gear-up landing. The purpose of the accident flight was to ferry the airplane to a nearby airport to receive an annual inspection after completion of the repairs. On the morning of the accident, a mechanic taxied the airplane and performed an engine run-up; he did not note any anomalies. The pilot fueled the airplane and started the engine for the flight. Upon starting, the engine went immediately to full power, where it remained as the airplane taxied at high speed about 1,000 ft into a tree. Witnesses reported that the pilot was awake and alert after the accident; thus, there was no evidence of pilot incapacitation. Examination of the wreckage did not reveal any preimpact mechanical malfunctions or anomalies. Based on the positions of the throttle and mixture control, and the high speed taxi after engine start, it is likely that the pilot started the engine with the throttle lever accidently in the full-forward position. After the engine started, the pilot could have reduced or ceased engine power by retracting the throttle, retracting the mixture, or turning the magnetos off.
Probable Cause: The pilot's improper engine start procedure, which resulted in a loss of control on the ground and collision with a tree.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA17LA042 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N8849H https://flightaware.com/photos/view/269247-28ea296602bd5daaef021e48aa35808d8168980b/aircraft/N8849H/sort/votes/page/1/size/vga Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
10-Nov-2016 18:36 |
Geno |
Added |
01-May-2018 13:45 |
ASN Update Bot |
Updated [Total fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
01-May-2018 14:07 |
harro |
Updated [Time, Source, Narrative, Photo, ] |
21-Jun-2021 15:27 |
Anon. |
Updated [Aircraft type] |
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