Wirestrike Accident Advanced Aeromarine Buccaneer IIB N696FT,
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ASN Wikibase Occurrence # 192844
 
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Date:Saturday 14 January 2017
Time:17:15
Type:Silhouette image of generic BUCA model; specific model in this crash may look slightly different    
Advanced Aeromarine Buccaneer IIB
Owner/operator:Private
Registration: N696FT
MSN: B2B005 582
Year of manufacture:1992
Total airframe hrs:948 hours
Engine model:Rotax
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Suwannee River, near Luraville, FL -   United States of America
Phase: Take off
Nature:Private
Departure airport:Mayo, FL
Destination airport:Mayo, FL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The sport pilot of the experimental, amateur-built, amphibious airplane flew to meet a friend to camp for the night along a river. He landed on the river to the north, flying over power lines during the landing approach, and pulled the airplane onto the shore. The pilot offered to help his friend search for a life vest that had floated downstream after he finished unloading the gear from the airplane. Multiple witnesses watched as the pilot departed northbound on the river, made a 180° turn southbound, then flew over the river, beneath treetop level, and out of sight. They reported hearing a loud "boom" and the engine noise stop just before a power outage occurred. One witness reported seeing the airplane flying 30-40 ft above the river when it "suddenly flipped backwards and then hit the water." One witness reported that the sky was grey and overcast, and that the sun was setting about the time of the accident, making the power lines difficult to see. The powerlines directly overhead of the accident site displayed striations consistent with the airplane impacting the powerlines.

Examination of the wreckage revealed no evidence of a preexisting anomaly or malfunction that would have precluded normal operation. Toxicology testing on the pilot detected two medications, which were unlikely to have caused impairment, and the autopsy revealed an enlarged heart; however, there was no evidence of a heart attack or any other incapacitating event. It is likely that, while flying along the river at low altitude, the pilot failed to see the powerlines, which resulted in an in-flight collision with the powerlines and impact with the river.

Probable Cause: The pilot's failure to see and avoid power lines while flying at low altitude.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA17FA088
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=696FT

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
15-Jan-2017 02:24 Geno Added
15-Jan-2017 18:01 Aerossurance Updated [Location]
15-Jan-2017 18:02 Aerossurance Updated [Location, Narrative]
16-Jan-2017 13:08 CaptainCrunch Updated [Aircraft type]
16-Jan-2017 18:22 Cracklow Updated [Registration, Source, Damage]
16-Jan-2017 18:23 harro Updated [Aircraft type, Cn, Operator]
16-Jan-2017 21:05 Geno Updated [Phase, Nature, Source, Narrative]
01-Jun-2018 09:56 ASN Update Bot Updated [Time, Nature, Departure airport, Destination airport, Source, Narrative]
01-Jun-2018 11:49 harro Updated [Source, Narrative, Photo, ]

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