Accident Beechcraft B19 Musketeer Sport N18925,
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ASN Wikibase Occurrence # 195277
 
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Date:Monday 8 May 2017
Time:10:00
Type:Beechcraft B19 Musketeer Sport
Owner/operator:Hyde Flight School
Registration: N18925
MSN: MB-872
Year of manufacture:1977
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Parker County, SW of Weatherford, TX -   United States of America
Phase: Landing
Nature:Training
Departure airport:Granbury, TX (GDJ)
Destination airport:Weatherford, TX
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor stated that a preflight visual inspection of the airplane’s fuel tanks indicated that the fuel in each tank was just above the tabs, which corresponded to 30 total gallons of fuel on board; he added that a pretakeoff engine run up revealed no anomalies. He and the student pilot then departed on the instructional flight and flew for about 30 minutes using fuel from the left fuel tank before switching to the right tank. The student reported that, when they switched fuel tanks, the left tank gauge indicated “just above half” full, and the right tank gauge indicated “slightly higher” than half full. Shortly thereafter, the student activated the carburetor heat and reduced engine power to idle to perform a simulated engine failure and forced landing; however, when the student applied the throttle at the conclusion of the simulation, engine power did not increase. The flight instructor performed a forced landing, during which the airplane impacted a tree.
Postaccident examination of the airplane revealed that the fuel selector was positioned to the left fuel tank, which was undamaged and contained no fuel. The right fuel tank contained about 14 gallons of fuel. The fuel lines from the engine firewall to the carburetor did not contain fuel. The fuel quantity transmitters were not tested, and their accuracy was not determined. No mechanical anomalies were noted that would have precluded normal operation of the airplane, and the loss of engine power is consistent with fuel starvation.
 


Probable Cause: The flight instructor’s inadequate in-flight fuel management, which resulted in fuel starvation and a total loss of engine power.
 

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN17LA179
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=18925

Location

Revision history:

Date/timeContributorUpdates
08-May-2017 21:42 Geno Added
09-May-2017 15:06 Geno Updated [Aircraft type, Registration, Cn, Operator, Source]
11-Nov-2018 08:35 ASN Update Bot Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative, Accident report, ]

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