ASN Wikibase Occurrence # 195325
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Date: | Thursday 2 March 2017 |
Time: | 16:38 UTC |
Type: | de Havilland Canada DHC-8-202Q Dash 8 |
Owner/operator: | Air Greenland |
Registration: | OY-GRO |
MSN: | 482 |
Fatalities: | Fatalities: 0 / Occupants: 29 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Kangerlussuaq-Søndre Strømfjord Airport (SFJ/BGSF) -
Greenland
|
Phase: | Take off |
Nature: | Passenger - Scheduled |
Departure airport: | Kangerlussuaq-Søndre Strømfjord Airport (SFJ/BGSF) |
Destination airport: | Sisimiut Airport (JHS/BGSS) |
Investigating agency: | HCLJ |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Air Greenland flight GL235 was involved in a serious runway incursion incident on takeoff from Kangerlussuaq Airport in Greenland.
The aircraft, a DHC-8-200 was scheduled to depart for Sisimiut, Greenland at 15:35 UTC. The flight was about an hour late when it received taxi instructions at 16:36 UTC.
The Sondrestrom Tower (TWR) controller cleared the flight to line up on runway 27 via taxiway A. The flight crew of OY-GRO read back the taxi instructions.
Sondrestrom TWR then instructed three runway snow clearing vehicles to vacate runway 27.
The flight crew of OY-GRO lined up the aircraft on runway 27 and completed the before take-off checklist. The flight crew was in doubt about whether or not a take-off clearance had been issued but agreed that the aircraft was cleared for take-off.
There was no visual contact with the three runway snow clearing vehicles on runway 27 because of the runway downslope.
The student air traffic controller at Sondrestrom TWR observed that OY-GRO had started its take-off roll and pointed it out to the instructor air traffic controller. For a short while, the instructor air traffic controller considered an instruction on aborting the take-off roll of OY-GRO, but noticed that OY-GRO started rotating.
When OY-GRO rotated, the horizontal separation to the nearest runway snow clearing vehicle on the runway was approximately 900 meters. The vertical separation, when OY-GRO passed overhead the nearest runway snow clearing vehicle on the runway, was approximately 300 feet.
CONCLUSIONS:
OY-GRO departed from an engaged runway at BGSF without an ATC take-off clearance.
To the AIB, the following combined conditions had an influence on the sequence of events:
- The actual flight was approximately one hour behind the scheduled time of departure.
- An over-motivated flight crew acted from their expectations rather than the factual reality.
- Runway downslope prevented the flight crew from spotting the three runway snow clearing vehicles.
- Soft safety barriers like the applied ATC phraseology and the flight crew standard operating procedures on use of landing lights did not provoke or raise the attention of the flight crew in such a way that their decision making process changed.
Accident investigation:
|
| |
Investigating agency: | HCLJ |
Report number: | |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
http://havarikommissionen.dk/index.php?option=com_contentbuilder&title=search-aviation-hclj510-2017-324-bulletin&controller=details&id=4&record_id=672&Itemid=225&limitstart=0&filter_order=&lang=en
History of this aircraft
Other occurrences involving this aircraft
25 June 1999 |
VH-SDA |
Sunstate Airlines |
0 |
Approx. 220NM NW of Cairns, QLD |
|
min |
Images:
Revision history:
Date/time | Contributor | Updates |
11-May-2017 19:16 |
harro |
Added |
11-May-2017 19:27 |
harro |
Updated [Narrative, Photo, ] |
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