ASN Wikibase Occurrence # 197429
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Date: | Thursday 10 August 2017 |
Time: | 16:14 |
Type: | Cirrus SR22T |
Owner/operator: | Private |
Registration: | N702N |
MSN: | 1494 |
Year of manufacture: | 2017 |
Total airframe hrs: | 165 hours |
Engine model: | Continental TSIO-550-K |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Raton Municipal Airport/Crews Field (KRTN), Raton, NM -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Eldorado, AR (ELD) |
Destination airport: | Raton, NM (RTN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot reported that he was checking weather conditions every hour during the personal, cross-country flight. While approaching the destination airport, he had to maneuver around convective activity about 10 miles northwest of the airport. While the airplane was on approach and about 4 miles from the airport, the local fix-based operator announced on the UNICOM that the winds were from 170° at 7 knots. The airplane crossed the runway 20 threshold about 85 knots and with full flaps. About 15 ft from touchdown, the airplane began to sink rapidly. The pilot attempted to arrest the descent, but the airplane impacted the runway and bounced, and wind began to push the airplane hard to the left. The pilot then initiated a go-around with full throttle and pulled back on the stick. The airplane climbed to between about 15 and 20 ft above ground level, the stall warning sounded, and the right wing stalled and then dropped. The airplane then struck an embankment off the right side of the runway and rolled onto its right side.
A review of weather information showed that a wind shift occurred about 2 minutes before landing, at which time, the reported winds were from 180° at 12 knots. The pilot reported that he believed that there was wind shear.
Probable Cause: The pilot's failure to maintain a proper descent rate, which resulted in a bounced landing, and his subsequent failure to attain a proper airspeed during an attempted go-around in shifting wind conditions, which resulted in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA359 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N702N FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N702N Location
Revision history:
Date/time | Contributor | Updates |
12-Aug-2017 15:05 |
Geno |
Added |
19-Apr-2020 17:28 |
ASN Update Bot |
Updated [Time, Operator, Total occupants, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
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