ASN Wikibase Occurrence # 198562
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Date: | Tuesday 23 August 2016 |
Time: | 09:46 |
Type: | Cessna T207 Turbo Skywagon |
Owner/operator: | Smokey Bay Air Inc |
Registration: | N91025 |
MSN: | 20700016 |
Year of manufacture: | 1969 |
Total airframe hrs: | 4536 hours |
Engine model: | Continental IO-550-F12B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Nanwalek, AK -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Port Graham, AK (PGM) |
Destination airport: | Nanwalek, AK (KEB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during landing the wind sock at the airport indicated that the wind was variable, about 5 knots, and predominately favored runway 1.
According to the FAA airport facility directory, runway 01/19 was 1,850 feet long, and soft gravel. However, 1,000 feet of northern portion of the runway was closed indefinitely.
The pilot recalled that about 500 feet down the 1,850 foot runway, and just before touchdown the airplane encountered, “a pretty rapid shift in the winds in both direction and velocity.” He reported that the airplane touched down momentarily, and then went airborne again. After the second touchdown, the speed did not decline as expected, and although the airplane did start to slow as it got a better grip on the gravel (which was wet from rain that had occurred earlier), he ran out of runway. He reported that the airplane overran the runway at a groundspeed of about 10 knots, went down a small embankment, had a propeller strike and the airplane sustained substantial damage when the left wing struck a post.
The pilot reported that there were no mechanical malfunctions or anomalies during the flight that would have prevented normal flight operations.
The pilot reported that he considered going around, but due to the wind and terrain rejected the idea.
Probable Cause: The pilot’s unstabilized approach and a subsequent runway overrun while landing on a short runway in variable wind conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA16CA445 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 08:11 |
ASN Update Bot |
Added |
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