ASN Wikibase Occurrence # 198733
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 27 October 2014 |
Time: | 16:04 |
Type: | Eurocopter AS 350B2 Ecureuil |
Owner/operator: | U.S. Department of Homeland Security |
Registration: | N5204X |
MSN: | 3099 |
Year of manufacture: | 1998 |
Total airframe hrs: | 5781 hours |
Engine model: | Turbomeca Arriel 1D1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bisbee, AZ -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | Fort Huachuca/Sierra Vista Municipal Airport, AZ (FHU/KFHU) |
Destination airport: | Fort Huachuca/Sierra Vista Municipal Airport, AZ (FHU/KFHU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was maneuvering the turbine engine-equipped helicopter about 25 ft above ground level when the engine suddenly experienced a total loss of power. The pilot performed an autorotation, and the helicopter touched down hard and rolled over, coming to rest inverted. Examination of the engine revealed that the pneumatic control pipe (P2), which delivers air pressure from the centrifugal compressor on the engine to the fuel control unit (FCU), was disconnected at the engine fitting. The loss of P2 pressure to the FCU resulted in the FCU commanding the engine to spool down to ground idle speed by limiting the fuel flow. There was no evidence of malfunctions or anomalies on the pipe, threads, and union fastener. There was no evidence of torque stripe residue on the disconnected fitting, consistent with the likely scenario that, during past maintenance, the B-nut was not properly torqued and gradually vibrated off its attach fitting while in flight.
The engine manufacturer had several caution notifications within multiple maintenance task documents to prevent removal of the P2 pipe during washing and the risk of an engine failure due to insufficient torque.
Probable Cause: Failure of maintenance personnel to ensure adequate torque of a pneumatic control pipe (P2) fitting, which resulted in a loss of engine power during low altitude flight maneuvers.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR15TA027 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 14:55 |
ASN Update Bot |
Added |
01-Jun-2023 11:19 |
Ron Averes |
Updated |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation