ASN Wikibase Occurrence # 198866
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Date: | Thursday 7 April 2011 |
Time: | 11:45 |
Type: | Piper PA-32-300 |
Owner/operator: | Private |
Registration: | N31407 |
MSN: | 32-7840130 |
Year of manufacture: | 1978 |
Total airframe hrs: | 3051 hours |
Engine model: | Lycoming IO-540 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oklahoma City, OK -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Oklahoma City, OK (HSD) |
Destination airport: | Oklahoma City, OK (HSD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane nosed over shortly after takeoff and impacted the runway. The nose landing gear collapsed and the airplane sustained substantial damage to the firewall. A postaccident examination revealed that a stabilator control cable had failed at a turnbuckle as a result of stress corrosion cracking, which compromised the pilot's ability to control the pitch attitude of the airplane. The airplane was within the maintenance inspection requirements at the time of the accident, with the most recent annual inspection being completed about 1 year prior to the accident. The airplane service manual included a special control cable fitting inspection for airplanes in service 15 years or more. Any evidence of corrosion or cracking was cause for replacement according to the service manual. The accident pilot had owned the airplane for about 26 years. During the time he owned the airplane, the control cables had not been replaced. The investigation could not determine when the stress corrosion cracking commenced on the turnbuckle.
Probable Cause: The loss of aircraft control due to the failure of the stabilator control cable turnbuckle.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11LA275 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 16:00 |
ASN Update Bot |
Added |
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