ASN Wikibase Occurrence # 201886
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Date: | Tuesday 5 January 1999 |
Time: | 11:10 LT |
Type: | Cessna 172M |
Owner/operator: | Mark Howell |
Registration: | N80253 |
MSN: | 172-66478 |
Total airframe hrs: | 8557 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Midlothian, TX -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Grand Prairie, TX (GPM |
Destination airport: | (4T6) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the FAA inspector who responded to the accident site, the 24 hour student pilot had flown with his flight instructor from the home base airport to a nearby uncontrolled airport for a supervised solo flight. After a few practice takeoffs and landings at the uncontrolled airport, the flight instructor exited the airplane and cleared the student pilot for a solo flight. The student pilot reported that while on short final for runway 18, 'he caught a gust of wind from the left which pushed the left wing up and banked the airplane to the right.' The student added that he applied full engine power to perform a go-around, yet the nose pitched down. The student stated that the airplane impacted the ground on the west side of the runway in a nose low attitude with the right wing down. The airplane came to rest in the inverted position, approximately 100 feet from the edge of the runway. The flaps were found extended approximately 15 degrees. The winds at the time of the accidents were estimated to be from 150 degrees at 15 knots, gusting to 20.
Probable Cause: The student pilot's failure to compensate for a crosswind resulting in a loss of control. Factors were the gusty high winds and the flight instructor's improper decision to allow the student to solo during high winds.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW99LA063 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB FTW99LA063
Location
Revision history:
Date/time | Contributor | Updates |
26-Nov-2017 09:37 |
ASN Update Bot |
Added |
08-Apr-2024 11:03 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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